N6319G

Substantial
Minor

Cessna 150KS/N: 15071819

Summary

On June 17, 2002, a Cessna 150K (N6319G) was involved in an accident near Seaman, OH. The accident resulted in 1 minor injury, with 1 person uninjured out of 2 aboard. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this accident to be: The pilot's failure to maintain airspeed during a precautionary landing, which resulted in an inadvertent stall/mush, and uncontrolled descent to the ground. A factor was the pilots' lack of recent experience.

On June 16, 2002, about 2000 eastern daylight time, a Cessna 150K, N6319G, was substantially damaged when it struck the ground during a precautionary landing in Seaman, Ohio. The certificated private pilot received minor injuries, and the passenger was not injured. Visual meteorological conditions prevailed for the local flight. No flight plan had been filed for the personal flight that was conducted under 14 CFR Part 91.

The pilot reported that he had a private airstrip located on his property, and intended to make a local flight. He inspected the airplane and departed to the northwest from the private airstrip. Climbing through about 400 feet above the ground, he observed and smelled smoke coming from under the instrument panel.

This accident is documented in NTSB report NYC02LA114. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N6319G.

Accident Details

Date
Monday, June 17, 2002
NTSB Number
NYC02LA114
Location
Seaman, OH
Event ID
20020625X00968
Coordinates
38.928890, -83.591392
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
1
Total Aboard
2

Probable Cause and Findings

The pilot's failure to maintain airspeed during a precautionary landing, which resulted in an inadvertent stall/mush, and uncontrolled descent to the ground. A factor was the pilots' lack of recent experience.

Aircraft Information

Registration
N6319G
Make
CESSNA
Serial Number
15071819
Engine Type
Reciprocating
Year Built
1970
Model / ICAO
150KC150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SHUPERT RONNIE D
Address
883 MOORES RD
Status
Deregistered
City
SEAMAN
State / Zip Code
OH 45679-9743
Country
United States

Analysis

On June 16, 2002, about 2000 eastern daylight time, a Cessna 150K, N6319G, was substantially damaged when it struck the ground during a precautionary landing in Seaman, Ohio. The certificated private pilot received minor injuries, and the passenger was not injured. Visual meteorological conditions prevailed for the local flight. No flight plan had been filed for the personal flight that was conducted under 14 CFR Part 91.

The pilot reported that he had a private airstrip located on his property, and intended to make a local flight. He inspected the airplane and departed to the northwest from the private airstrip. Climbing through about 400 feet above the ground, he observed and smelled smoke coming from under the instrument panel. The pilot immediately turned back toward the airstrip, and passed over the airstrip about 400 feet high. He then circled to come back for a landing, and as he turned the airplane to final approach, "it quite flying, and veered to the left." The pilot reported that the flight controls did not have any affect on the airplanes flight path. The pilot also reported that he thought the engine lost power about the same time as the airplane quit flying.

According to an inspector from the Federal Aviation Administration (FAA), the airplane touched down at the end of a level pasture, about 1,500 feet from the approach end of the runway. The airplane overran the level ground, and continued downhill for about 100 feet. The lower cowling was crushed up and rearward. The nose wheel fork was bent aft and to the right with the nosewheel separated from the nosewheel fork. The fuselage aft of the cabin was buckled to the left. One propeller blade was bent aft, and dirt was impacted on the leading edge of the bent blade. The top surface of the wings were wrinkled.

A follow-up inspection of the airplane was conducted by a certificated mechanic with the FAA inspector in attendance. According to the FAA inspector, finger compression was attained in all cylinders, and the magnetos operated normally. The "P" leads were attached and the magneto switch operated normally. The fuel strainer contained a small amount of sediment. The carburetor, venturi and associated parts were checked, and drained; and no abnormalities found. No evidence of burns or discoloration were found on any electrical wiring.

Oil was found leaking from the pushrods on both sides of the engine. Burned oil was found on the muffler. No other oil leakage was found.

During a telephone interview, the FAA inspector reported that fuel was found in both fuel tanks, and oil was found in the engine. With the spark plugs removed, the engine was rotated, with no evidence of binding.

The pilot reported that his total flight experience was 250 hours. He also reported that in the preceding 12 months, he had accumulated about 8 hours. In the preceding 6 months, he had flown the airplane once in February, and then again in June. There were three or four short flights in June, with a total accumulation of about 1 hour in the 90 days that preceded the accident flight.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC02LA114