N11LP

Substantial
Minor

Cessna 185BS/N: 1850574

Accident Details

Date
Sunday, August 4, 2002
NTSB Number
CHI02LA235
Location
Brainerd, MN
Event ID
20020813X01375
Coordinates
46.383335, -94.361946
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
2
Total Aboard
3

Probable Cause and Findings

The pilot's evasive maneuver to avoid obstacle clearance, resulting in a premature lift off with inadequate airspeed followed by a stall. The presence of the boat was a factor.

Aircraft Information

Registration
N11LP
Make
CESSNA
Serial Number
1850574
Engine Type
Reciprocating
Year Built
1963
Model / ICAO
185BC185
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
NORTHERN AIR SERVICE INC
Address
PO BOX 397
Status
Deregistered
City
MINONG
State / Zip Code
WI 54859-0397
Country
United States

Analysis

On August 4, 2002, at 1400 central daylight time, a float equipped Cessna 185B, N11LP, piloted by a private pilot, sustained substantial damage when it impacted the water and nosed over during takeoff from Gull Lake, near Brainerd, Minnesota. The 14 CFR Part 91 personal flight was operating in visual meteorological conditions without a flight plan. The pilot received minor injuries and the two passengers were not injured. The flight was originating at the time of the accident with Minong, Wisconsin, as the intended destination.

The pilot furnished no narrative description of the accident in the report submitted to the National Transportation Safety Board. The section of the report for describing mechanical malfunctions was checked "No."

The initial reports indicated that the airplane engine lost power during takeoff from the lake and the pilot attempted to land back on the lake. During the attempted landing the left wingtip struck the water first. The airplane subsequently flipped over coming to rest upside down.

A witness to the accident reported seeing and hearing the airplane during the accident sequence. The witness reported being in a boat that was pulling a water skier at the time of the accident. She said that the airplane lifted off of the water when it was about 30 feet behind the skier, climbed to 30 feet above the boat, turned sharply to the left and fell into the water. The witness stated that the airplane engine was running and was "really loud." She said that she saw no smoke or fire coming from the airplane prior to impact.

A second witness who was also in the boat said the airplane came over the boat and then "it just came down." She said that she heard engine noises from the airplane until it hit the water. She said that there was no smoke coming from the airplane prior to impact.

A postaccident examination of the airplane by Federal Aviation Administration officials revealled no pre-impact mechanical defects with respect to the airframe. The airplane's engine was retained and examined at the manufacturer's facility in Mobile, Alabama. The examination of the engine was performed under the direct supervision of a National Transportation Safety Board Investigator. No pre-impact defects that would have precluded engine operation were found during the examination of the engine.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI02LA235