N62897

Substantial
Minor

Boeing Stearman A75S/N: 75-6960

Accident Details

Date
Monday, November 11, 2002
NTSB Number
NYC03LA017
Location
Glade Spring, VA
Event ID
20021122X05509
Coordinates
36.779724, -81.733612
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

the pilot's improper in-flight decision to fly at an altitude that did not allow for successful completion of a forced landing, after the engine lost power for undetermined reason(s). A factor was the unsuitable terrain.

Aircraft Information

Registration
N62897
Make
BOEING STEARMAN
Serial Number
75-6960
Engine Type
Turbo-jet
Model / ICAO
A75B752
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
EAST WEST AVIATION CLUB
Address
C/O DONALD NORRIS
236 CROOKED HOLLOW RD
Status
Deregistered
City
ELGIN
State / Zip Code
TX 78621-5527
Country
United States

Analysis

On November 11, 2002, about 1440 eastern standard time, a Boeing Stearman A75, N62897, was substantially damaged during a forced landing in Glade Spring, Virginia. The certificated private pilot, and pilot rated passenger received minor injuries. Visual meteorological conditions prevailed for the local flight that originated from Abingdon, Virginia. No flight plan had been filed for the personal fight that was conducted under 14 CFR Part 91.

According to an inspector from the Federal Aviation Administration (FAA), the accident airplane was part of a three airplane formation that had conducted a fly-by at a nearby Veterans Day celebration. At the completion of the fly-by, the three airplanes headed back to Abingdon. In the vicinity of Glade Spring, while two airplanes continued on to Abingdon, the pilot of the accident airplane broke formation, and descended. Several witnesses observed the accident airplane performing low level flight, below the level of the surrounding hills. The pilot reported that the pilot rated passenger was not handling the flight controls at the time of the accident.

According to the pilot, he was maneuvering at a low altitude when the engine lost power, and could not clear a tree ahead of him. There was no suitable terrain that he could reach, and the airplane struck the tree, and came to rest inverted. The pilot reported that he added carburetor heat, moved the throttle, verified that the mixture was rich, and tried different positions on the magneto switch. but was unable to restore power to the engine. He also stated that the airplane had been operated for about one hour and the fuel tank was full at departure.

The FAA inspector reported that fuel was found in the fuel tank, the propeller was fragmented, the engine had separated from the airframe. The carburetor was crushed, and the fuel line that ran from the fuselage to the engine were separated, and no fuel remained in the line. The FAA inspector reported that he checked the fuel lines from the tank to the engine and there was no indication of obstructions in the lines. The upper and lower right side wings were destroyed, and the upper and lower left side wings had received substantial damage.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC03LA017