N4672D

Substantial
None

Shepherd Kolb Mark IIIS/N: 0100

Accident Details

Date
Thursday, November 28, 2002
NTSB Number
FTW03LA052
Location
Norfork, AR
Event ID
20030107X00032
Coordinates
36.165554, -92.144996
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The loss of engine power due to fuel contamination. Contributing to the accident were the trees.

Aircraft Information

Registration
N4672D
Make
SHEPHERD
Serial Number
0100
Engine Type
Reciprocating
Year Built
1996
Model / ICAO
Kolb Mark IIIBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SHEPHERD DALLAS E TRUSTEE
Address
983 SHEID RD
Status
Deregistered
City
NORFORK
State / Zip Code
AR 72658-8383
Country
United States

Analysis

On November 28, 2002, at 1456 central standard time, a Shepherd Kolb Mark III homebuilt experimental airplane, N4672D, registered to and operated by the pilot, was substantially damaged during a forced landing following a loss of power shortly after takeoff from a private grass airstrip near Norfork, Arkansas. The private pilot and his passenger were not injured. Visual meteorological conditions prevailed and a flight plan was not filed for the Title 14 Code of Federal Regulations Part 91 personal flight. The local flight was originating at the time of the accident.

The 350-hour pilot reported in the Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) that, prior to take off, he refueled the airplane with 28 gallons of 93-octane automotive fuel and checked the fuel sump for signs of contamination. After a normal takeoff, the engine "quit" approximately 100 feet AGL. Subsequently, the airplane descended into a tree line and came to rest upright.

The pilot reported that the airplane sustained structural damage to the cabin section of the fuselage and the right wing. He also reported that he found water in the carburetor bowl. Upon discovering water in the carburetor bowl, the pilot drained 26 gallons of fuel from the tank and found no visible signs of water. The pilot stated that he suspected that "fuel contamination" was the reason for the loss of engine power.

The pilot further reported to an FAA inspector who responded to the site of the accident, that the airplane had been flown for 5 hours in the past 90 days and the fuel tank was left half full for a "long time" before being filled prior to the day of the flight.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW03LA052