N842PS

Substantial
None

Piper PA24S/N: 24-4685

Accident Details

Date
Saturday, March 15, 2003
NTSB Number
LAX03LA113
Location
MESA, AZ
Event ID
20030321X00366
Coordinates
33.313056, -111.659164
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The flight instructor's delayed remedial action during a go-around, which resulted in an inadvertent touchdown and hard landing. Factors associated with the accident are a momentary loss of engine power, and the inadvertent touchdown.

Aircraft Information

Registration
N842PS
Make
PIPER
Serial Number
24-4685
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
PA24PA24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
ARIZONA CLOUDBUSTERS INC
Address
4302 E SILVERWOOD DR
Status
Deregistered
City
PHOENIX
State / Zip Code
AZ 85048-7444
Country
United States

Analysis

On March 15, 2003, at 0809 mountain standard time, a Piper PA24, N842PS, experienced a partial loss of engine power and inadvertently made hard contact with the runway surface at Memorial Airfield (34AZ), Chandler, Arizona. The flight continued to the Williams Gateway Airport (IAW), Mesa, Arizona, and landed gear up. Arizona Cloud Busters owned and operated the airplane under the provisions of 14 CFR Part 91. The certified flight instructor (CFI), a private pilot under instruction (PUI), and one passenger were not injured. Visual meteorological conditions prevailed for the local area practice flight, and no flight plan had been filed. The flight departed the Stellar Airpark (P19), Chandler, Arizona, at 0710.

According to both the CFI and PUI, the purpose of the flight was to practice commercial maneuvers for the PUI's upcoming commercial check ride.

The CFI stated that they conducted a preflight, and discussed how to handle an engine failure on takeoff. He stated that after takeoff, about 1,000 feet above ground level (agl), he simulated an engine failure by retarding the throttle. He noted no discrepancies with the recovery of the simulated engine failure. During the flight the CFI and student flew the airplane at various airspeeds and discussed the "best glide speeds for endurance versus range."

The plan at 34AZ was to simulate a loss of engine power, make an approach for landing, apply power, and complete a low approach over the field. When the student applied full power, there was no corresponding power increase for "several seconds." The CFI took the flight controls; however, the landing gear contacted the runway surface. At the time the landing gear contacted the surface, the engine "caught and developed full [rpm] in time for me to gain control and the [airplane] to gain altitude."

The CFI stated that they believed the landing gear was damaged. They flew to CHD, and tower personnel stated that the landing gear was not fully extended. The CFI and tower personnel discussed landing options. The CFI decided to land gear up at IAW due to the fact that their fire department had more equipment than CHD. After the fire equipment was in place, the CFI landed on runway 12 at IAW with the landing gear retracted, full flaps, and the engine shut down.

According to a Federal Aviation Administration (FAA) inspector who visually examined the airplane, there were multiple holes on the fuselage.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX03LA113