N48TA

Substantial
None

Beech E-90S/N: LW-283

Accident Details

Date
Thursday, January 8, 2004
NTSB Number
CHI04LA053
Location
Galesburg, IL
Event ID
20040112X00052
Coordinates
40.938056, -90.431114
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
7
Total Aboard
7

Probable Cause and Findings

The pilot's inadequate preflight by not complying with the airplane's before takeoff checklist to verify that the cabin door was secured leading to its in-flight separation from the airplane. A factor was that the door was not secured.

Aircraft Information

Registration
N48TA
Make
BEECH
Serial Number
LW-283
Engine Type
Turbo-shaft
Model / ICAO
E-90BE9L
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
KING INDUSTRIES CORP
Address
1210 MECHEM DR
Status
Deregistered
City
RUIDOSO
State / Zip Code
NM 88345-7206
Country
United States

Analysis

On January 8, 2004, about 1430 central standard time, a Beech E-90, N48TA, operated by Tidewater Aero, sustained substantial damage when the cabin door opened in-flight and impacted the empennage during climb out near Galesburg, Illinois. The non-scheduled domestic passenger flight was operating under 14 CFR Part 135. Visual metrological conditions prevailed at the time of the accident. An instrument flight rules (IFR) flight plan was on file. The airline transport pilot and his six passengers reported no injuries. The flight originated at the Galesburg Municipal Airport (GBG), near Galesburg, Illinois, about 1425, and was destined for Mountain Empire Airport, near Marion, Virginia.

The accident report, signed by the pilot, stated:

At 1415 CST N48TA was loaded with one pilot, [pilot's name],

PIC [pilot-in-command], for Tidewater Aero, two Virginia Beach

(VA BCH) police officers, and [four] prisoners, being returned

to VA BCH. The PIC was among the first aboard. A VA BCH

police officer closed the aircraft door, while the PIC was in the

cockpit. The door was not verified to be closed properly by

the PIC. At 1425 CST, the aircraft departed [runway] 21 at GBG

and started a climbing left turn. At approximately 2000 [feet]

MSL, the "Cabin Door" annunciator light came on. At that point

the PIC turned the aircraft further left to return to GBG for landing.

Power was reduced, and the climb stopped. At [approximately]

1430 CST, 2 [miles southeast] of GBG, the door separated from

the aircraft. ... Witness sitting at the side facing seat-opposite from

the door said he could hear loud "air" noise coming from the door

before it separated. Aircraft was in a left turn when the door

separated. Upon returning to GBG, ground crew brought a ladder

to unload passengers without incident.

That report stated that "no one on board or on the ground was injured" and it listed no mechanical malfunctions in reference to the flight.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI04LA053