N493RA

Substantial
None

Cessna 150-GS/N: 15066987

Accident Details

Date
Wednesday, April 28, 2004
NTSB Number
FTW04LA121
Location
Livingston, TX
Event ID
20040513X00598
Coordinates
30.684722, -95.017219
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A loss of engine power due to the blockage of the fuel system vents, resulting in fuel starvation. A contributing factor was the lack of suitable terrain for the forced landing.

Aircraft Information

Registration
N493RA
Make
CESSNA
Serial Number
15066987
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
150-GC150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
REGISTRATION PENDING
Address
100 PALMER LN
Status
Deregistered
City
COLDSPRING
State / Zip Code
TX 77331-4342
Country
United States

Analysis

On April 28, 2004, at 1800 central daylight time, a Cessna 150G, single-engine airplane, N493RA, registered to and operated by a private individual, sustained substantial damage during a forced landing following a loss of engine power while maneuvering in the vicinity of Livingston, Texas. The private pilot and one passenger were not injured. Visual meteorological conditions prevailed and a flight plan was not filed for the 14 Code of Federal Regulations Part 91 personal flight. The local flight originated from the Livingston Municipal Airport (00R), Livingston, Texas, at 1705.

According to the 175-hour pilot, after take off he climbed to approximately 1,000 feet above ground level (agl), and flew in the local area about 50 minutes. After making several circles around the airport, the engine started to run "rough." The pilot applied carburetor heat and maneuvered the airplane to set up for a forced landing into a field. He reported that the engine "appeared" to be starved from gas, and as he cycled the throttle, the engine would "restart." After several attempts to maintain engine RPM, the engine "quit." Subsequently, the pilot landed the airplane in a grassy field located across from the airport. During the roll-out, the front tire struck a small ditch, nosed-over, and came to rest inverted.

An examination of the wreckage by a Federal Aviation Administration (FAA) inspector, who responded to the accident site, revealed that the firewall was buckled. Both wing fuel caps appeared to have their respective vents "painted over," and when low pressure air was introduced to the left wing fuel vent, the vent appeared to be blocked. Higher pressure air was applied to the vent, and a "pop" was heard, as if the vent had "cleared" debris when the air was applied.

According to entries in the airplane's maintenance logbooks, the last annual inspection was completed on March 15, 2003. Additional entries showed that the airplane had flown a total of approximately 1.4 hours (including the 50 minutes of the accident flight) since the annual inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# FTW04LA121