N404DK

Substantial
None

North American T-28CS/N: 140461

Accident Details

Date
Friday, June 4, 2004
NTSB Number
CHI04LA147
Location
Manitowoc, WI
Event ID
20040610X00782
Coordinates
44.128887, -87.680557
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Failure of the number 4 piston articulating rod resulting in a complete loss of engine power during initial climb. The ditch was a contributing factor.

Aircraft Information

Registration
Make
NORTH AMERICAN
Serial Number
140461
Engine Type
Reciprocating
Year Built
1956
Model / ICAO
T-28CT28
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
T-28C

Registered Owner (Current)

Name
KALEMBER DUANE D
Address
3788 S LEE POINT RD
City
SUTTONS BAY
State / Zip Code
MI 49682-9616
Country
United States

Analysis

On June 4, 2004, about 1820 central daylight time, a North American T-28C, N404DK, owned and piloted by an airline transport pilot, was substantially damaged during a forced landing following a loss of engine power shortly after takeoff from runway 35 (5,000 feet by 100 feet, asphalt) at the Manitowoc County Airport (MTW), Manitowoc, Wisconsin. The flight was operating under 14 CFR Part 91 and was not on a flight plan. Visual meteorological conditions prevailed. The pilot reported no injuries. The local flight was originating at the time of the accident.

The pilot stated that as he was reducing to climb power after takeoff, about 200 feet above ground level, he felt a severe vibration and heard several "bangs." He reported that the engine "wound down". He made a slight left turn toward an open field adjacent to a barn to set up for a gear-up forced landing. He noted that the touchdown was smooth and the aircraft slid for approximately 335 feet. The aircraft yawed as it slid and came to a stop when the tail struck a ditch adjacent to a roadway.

A post-accident examination determined that the #4 articulating rod had failed resulting in the engine failure. The pilot reported that the engine had accumulated 10,005 hours total time, with 11.4 hours since overhaul.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI04LA147