N4585F

Substantial
None

Cessna 185FS/N: 1851092

Accident Details

Date
Thursday, June 24, 2004
NTSB Number
SEA04LA117
Location
Bozeman, MT
Event ID
20040702X00902
Coordinates
45.778057, -111.157501
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The failure of the right main gear brake disk attach flange during the landing roll, due to fatigue cracks emanating from numerous corrosion pits present on the surface of the disk, leading to the right brake becoming totally inoperative, and resulting in a rapid inadvertent ground-loop. Factors include hard braking applied by the pilot in order to turn off the active runway at an early taxiway, and considerable corrosion on the surface of the brake disk flange.

Aircraft Information

Registration
N4585F
Make
CESSNA
Serial Number
1851092
Engine Type
Reciprocating
Year Built
1966
Model / ICAO
185FC185
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CHAPMAN KENNETH D
Address
4906 E 15TH AVE
Status
Deregistered
City
SPOKANE VALLEY
State / Zip Code
WA 99212-3408
Country
United States

Analysis

On June 24, 2004, approximately 1510 mountain daylight time, a Cessna 185F, N4585F, ground-looped during the landing roll at Gallatin Field, Bozeman, Montana. The private pilot and his passenger were not injured, but the aircraft, which is owned and operated by the pilot, sustained substantial damage. The 14 CFR Part 91 personal pleasure flight, which departed from an unknown location, was being operated in visual meteorological conditions. No flight plan had been filed.

According to the pilot, during the landing roll he was applying normal heavy braking in order to turn off the runway at taxiway Echo, when the aircraft suddenly and rapidly ground-looped to the left. An initial post-accident inspection of the aircraft revealed that the right main gear brake rotor assembly had torn lose from the wheel itself, rendering the right wheel brake totally inoperative.

The wheel hub and brake disk assembly were shipped to the NTSB Materials Laboratory, where it was determined that the brake disk attachment flange failed in fatigue in the bend around the attachment flange. The brake disk showed a substantial amount of general corrosion, and although the attachment flange met the minimum thickness requirements, most of its surface was covered by corrosion and corrosion pitting. The fatigue crack propagation that eventually lead to the failure had originated in one of these corrosion pits.

The pilot did not return a completed NTSB Form 6120.1/2, so the total flight time information for this report was taken from data recorded on his last FAA medical examination.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA04LA117