N5015K

Substantial
None

Air Tractor AT-602S/N: 602-0429

Accident Details

Date
Monday, April 4, 2005
NTSB Number
CHI05LA088
Location
Imperial, NE
Event ID
20050408X00429
Coordinates
40.510276, -101.620002
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's inadequate preflight planning which led to fuel exhaustion and subsequent loss of engine power. The soft ground was a factor.

Aircraft Information

Registration
Make
AIR TRACTOR
Serial Number
602-0429
Engine Type
Turbo-prop
Model / ICAO
AT-602AT6T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
AT-602

Registered Owner (Current)

Name
WILLIAMS ERIC LYLE
Address
7425 FM 512
City
WOLFE CITY
State / Zip Code
TX 75496-2477
Country
United States

Analysis

On April 4, 2005, about 1025 mountain daylight time, an Air Tractor AT-602, N5015K, piloted by a commercial pilot, was substantially damaged during a forced landing following a loss of engine power while on approach to runway 31 at the Imperial Municipal Airport (IML), Imperial, Nebraska. The 14 CFR Part 137 flight was operating in visual meteorological conditions without a flight plan. The pilot was not injured. The local flight originated about 0928.

According to a report filed by the pilot, he had completed spray operations at a field located about 12 miles south of IML and was returning. He stated that according to the fuel flow meter he had about 40 minutes of fuel remaining when he exited the last field sprayed. He stated that when he was about 1 mile south of the airport, the engine lost power. He checked the fuel flow meter which "suggested" he had over 30 minutes of fuel remaining with 1/4 in one tank and 1/8 in the other tank. He stated that he executed a landing to a field and the main landing gear sunk into the soft dirt and the airplane nosed over.

Post accident examination of the airplane by Federal Aviation Administration inspectors revealed that some fuel had drained from the right wing fuel vent due to the position of the airplane. No other evidence of fuel leakage was detected. When the airplane was righted, no useable quantity of fuel was noted in the fuel tanks.

Subsequent to the accident, the airplane's engine was removed from the airplane and a functional test performed. The engine was run on a test stand and no anomalies were found with respect to the engine.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI05LA088