N7342P

Substantial
Fatal

Piper PA-24-250S/N: 24-2521

Accident Details

Date
Thursday, August 18, 2005
NTSB Number
LAX05FA271
Location
Pomona, CA
Event ID
20050901X01368
Coordinates
34.033611, -117.820274
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
2
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
3

Probable Cause and Findings

A loss of engine power during the landing approach due to fuel starvation caused by debris and corrosion in the carburetor assembly. A factor contributing to the accident was the failure of the owner to comply with the manufacturer's service bulletin regarding overhaul of the carburetor.

Aircraft Information

Registration
N7342P
Make
PIPER
Serial Number
24-2521
Engine Type
Reciprocating
Year Built
1961
Model / ICAO
PA-24-250PA24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SHEAR JAMES L
Address
13535 SAN ANTONIO AVE
Status
Deregistered
City
CHINO
State / Zip Code
CA 91701
Country
United States

Analysis

HISTORY OF FLIGHT

On August 17, 2005, about 1950 Pacific daylight time, a Piper PA-24-250, N7342P, impacted flat terrain at the Spadra Ranch facility for California Polytechnic State University, Pomona, California. The pilot/owner operated the airplane under the provisions of 14 CFR Part 91 as a personal flight. The airplane sustained substantial damage. The pilot and one passenger were fatally injured. A passenger seated in a back seat sustained serious injuries. Visual meteorological conditions prevailed for the local area flight, and no flight plan had been filed. The flight departed Zamperini Field Airport (TOA), Torrance, California, at an undetermined time. The flight's destination was Chino Airport (CNO), Chino, California.

A witness in his backyard heard an airplane's engine 'sputtering and cutting out.' When he looked up he saw the accident airplane flying 'really low' in an easterly direction. He did not see any smoke or fire coming from the airplane. The airplane made a turn northbound, and then returned to a southbound heading. As the airplane continued to circle he could no longer hear the engine. The witness reported that the airplane was "going down" and gliding towards a field. He lost sight of the airplane behind the tree line and then heard it crash. He responded to the accident site and observed the rear seated passenger standing on the passenger side wing. The witness could smell gas and told the passenger to "get away." The passenger told the witness that they were headed towards Chino, but did not indicate what had happened.

The National Transporation Safety Board investigator-in-charge (IIC) reviewed communications between the pilot and Brackett airport (POC) Air Traffic Control Tower personnel. At 1948, the pilot made the initial call to POC. A minute later the pilot reported an engine failure near San Antonio College (Mount Sac), about 5.5 miles from the airport. At 1950, the controller calls emergency equipment after he receives no response to his radio communications to the pilot. The controller further reported in his personnel statement that he coordinated with Pomona Air 1 to locate the airplane. The POC controller last observed the position of the accident airplane utilizing DBRITE (Digital Bright Radar Indicator Tower Equipment) about 3 miles southwest of the airport.

PERSONNEL INFORMATION

A review of Federal Aviation Administration (FAA) airman records revealed the pilot held a private pilot certificate with an airplane single and multiengine land ratings.

The pilot held a third-class medical certificate issued on September 27, 2004. It had the limitations that the pilot must wear corrective lenses.

The aeronautical experience listed in this report was obtained from a review of the airmen FAA records on file in the Airman and Medical Records Center located in Oklahoma City, Oklahoma. These records indicated a total time of 3,200 hours, with 50 hours logged in the last 6 months.

AIRCRAFT INFORMATION

The airplane was a 1961 Piper PA-24-250, serial number 24-2521. A review of the airplane's logbooks revealed a total airframe time of 3,760.60 hours at the last annual inspection. An annual inspection was completed on August 6, 2004. The entry for the annual inspection stated in part that the mechanic had to tighten some of the electrical leads on system. There were no other discrepancies identified during the annual inspection. The tachometer read 3,841.32 at the accident scene.

The airplane was equipped with a Textron Lycoming O-540-A1D5 engine, serial number L-18544-40. Total time on the engine at the last annual inspection was 3,760.60 hours. An engine field overhaul had been completed on June 24, 1993, with an engine total time of 1,098.2 hours.

A Marvel-Schebler, MA-4-5 carburetor, serial number R-41-9230, had been installed on the airplane. Service Bulletin MSA-3 Revision 1 dated November 18, 1991, titled Overhaul Periods for Float Carburetors, as issued by Precision Airmotive, LLC, indicated that the accident airplane's carburetor should be overhauled at the engine manufacturer's specified time between overhaul or 10 years in service or last overhauled, whichever occurs first. There were no airframe or engine logbook entries of compliance with Service Bulletin MSA-3 Rev. 1.

WRECKAGE AND IMPACT INFORMATION

The airplane impacted in a fallow field (Spadra Farm Field) owned by the State of California - Cal Poly Pomona University. The accident site was on the west side of Lanterman State Hospital in Pomona. Responding officers from the Cal Poly-Pomona Police Department noted a strong odor of fuel from the airplane when they arrived on scene. Officers also reported that the pilot and front passenger remained inside the airplane and that both occupants were wearing their "lap seatbelts." The rear seat passenger was outside of the airplane when the officers arrived, and they rendered assistance until the passenger was transported to a local area hospital. The passenger relayed to an officer that they had departed from the Torrance airport en route to Chino. The passenger did not indicate the nature of the emergency that precipitated the accident.

Investigators from the Safety Board, the FAA, Piper, and Textron Lycoming, parties to the investigation, responded to the accident site and examined the wreckage. The wreckage was at a Global Positioning System (GPS) coordinates of 34 degrees 02.023 minutes north latitude and 117 degrees 49.215 minutes west longitude. The debris path was along a magnetic bearing of 057 degrees.

The first identified point of contact (FIPC) was on a magnetic heading of 118 degrees, and the airplane came to rest upright 122 feet from the FIPC. The empennage partially separated from the aft cabin bulkhead and remained intact, and next to the cabin area. The engine remained attached to the engine mounts, firewall, and airframe; however, it was canted in a nose down attitude with the aft portion of the engine propped up against the instrument panel. The cockpit area of the airplane had been breached during the accident sequence. Three feet of the outboard section of the left wing came to rest about 45 feet from the main wreckage. The aft portion of the airplane had separated along the aft baggage door line and was slightly perpendicular to the fuselage.

The propeller assembly remained connected at the crankshaft flange. Both blades were bent near the hub and folded aft. The carburetor had been displaced from the engine; however, it remained intact. After the carburetor was removed, the throttle lever was manually actuated with a discharge of a steady stream of fuel from the accelerator discharge tube. The carburetor was disassembled and investigators noted contaminates at the bottom of the carburetor bowl. The float assembly remained in place and was not damaged.

Investigators visually inspected the airplane's fuel tanks and observed fuel in both right fuel tanks, which they estimated to be about 3/4 full. The left fuel tanks had been breached; however, the fuel bladder material was slick to the touch.

MEDICAL AND PATHOLOGICAL INFORMATION

The County of Los Angeles Department of Coroner, Los Angeles, California, conducted an autopsy on the pilot on August 21, 2005. The cause of death was listed as multiple blunt force trauma.

The TC FAA Forensic Toxicology Research Team, Oklahoma City, Oklahoma, performed a toxicological analysis from samples obtained during the autopsy. The tests for carbon monoxide and cyanide were not performed. The results of the analysis of the specimens were negative for volatiles and tested drugs.

According to the airplane manufacturer, when the airplane was delivered new in 1961, it had not been equipped with a shoulder harness restraint system. The airplane manufacturer indicated that a mandatory Service Bulletin No. 980 titled Should Harness Installation, dated January 18, 1995, existed for the accident make and model airplane, as well as several other models of Piper airplanes. During the on scene inspection, investigators found brand new uninstalled shoulder harnesses in the debris field.

The autopsy report for the pilot noted the following injuries under "Anatomical Summary":

A. Multiple blunt force trauma:

1. Abrasions/lacerations, face, neck, chest, abdomen and extremities

2. Multiple fractures, mandible/maxillae, sternum, ribs (left number 2 through number 12; right number 2 through number 5), T2-3 vertebrae.

3. Atlanto-occipital dislocation

4. Lacerations, aorta, left lung and liver

The front seat passengers' injuries were listed in part under the "Anatomical Summary" as:

B. Multiple blunt force trauma:

1. Abrasions/contusions/lacerations, head, face, neck, chest, abdomen and extremities.

2. Multiple fractures, basal skull (hinge-type), sternum, right ribs, and left tibia-fibula

3. Contusions/lacerations, brain and right lung

4. Subdural hemorrhage

TESTS AND RESEARCH

Investigators examined the wreckage at Aircraft Recovery Service, Littlerock, California, on August 19, 2005. Flight control continuity was established during the airframe examination, with no discrepancies noted with the airframe during the examination.

Investigators noted that the carburetor exhibited signs of previous water contamination as evidenced by rust and corrosion deposits inside the carburetor bowl, fuel pump, and gascolator bowl. Foreign object debris was also found in the main jet passage and carburetor bowl. According to the engine manufacturer's representative, the steel drain plug in the carburetor bowl had been severely corroded on the interior surface. Sediment was found in carburetor bowl and debris was found in the main fuel jet passage.

The top spark plugs were removed. All of the spark plugs were secure at each position with their respective leads attached. The spark plug electrodes were clean with no mechanical deformation. The spark plug ele...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX05FA271