Summary
On May 02, 2006, a Bell 206B (N342WC) was involved in an incident near Vinita, OK. All 4 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's improper pre-flight planning, which resulted in a total loss of engine power due to fuel exhaustion. A contributing factor was the lack of suitable terrain for the forced landing.
The 164-hour private pilot reported that when the single-engine turbine powered helicopter was seven miles from the airport, the fuel boost pump caution light illuminated and the fuel gauge was indicating approximately 15 gallons of fuel remaining. The pilot elected to continued to fly toward the airport; however, while on final approach the engine lost power. The pilot entered an autorotation, but due to his low altitude, he realized the descent angle would have placed the helicopter onto a busy four-lane highway. The pilot added that he increased the collective, which increased altitude, and he was able to cross over the highway and a fence; however, this maneuver reduced inertia in the main rotor system.
This incident is documented in NTSB report DFW06CA112. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N342WC.
Accident Details
Probable Cause and Findings
The pilot's improper pre-flight planning, which resulted in a total loss of engine power due to fuel exhaustion. A contributing factor was the lack of suitable terrain for the forced landing.
Aircraft Information
Registered Owner (Historical)
Analysis
The 164-hour private pilot reported that when the single-engine turbine powered helicopter was seven miles from the airport, the fuel boost pump caution light illuminated and the fuel gauge was indicating approximately 15 gallons of fuel remaining. The pilot elected to continued to fly toward the airport; however, while on final approach the engine lost power. The pilot entered an autorotation, but due to his low altitude, he realized the descent angle would have placed the helicopter onto a busy four-lane highway. The pilot added that he increased the collective, which increased altitude, and he was able to cross over the highway and a fence; however, this maneuver reduced inertia in the main rotor system. As a result, the pilot flared over a wet, grassy field about 30 feet, leveled the helicopter and landed with some forward speed. During touchdown, the skids dug into the ground and the helicopter came to an abrupt stop, toppled over, and came to rest upside down. The tail boom separated and came to rest about 20 feet from the fuselage. Examination of the helicopter revealed there was no fuel in the fuel nozzle or in the external fuel filter. There was no indication of a fuel spill during the mishap sequence.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW06CA112