N7043G

Destroyed
Fatal

Beech 65-A90-1S/N: LM-37

Accident Details

Date
Monday, June 12, 2006
NTSB Number
MIA06FA117
Location
Tampa, FL
Event ID
20060627X00837
Coordinates
27.922222, -82.459167
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The poor in-flight planning decision by the captain for his failure to establish the airplane on a stabilized approach for a forced landing, resulting in the airplane landing on a taxiway near the departure end of the runway. Contributing to the accident were the failure or malfunction of the primary hydraulic low pitch stop of both propellers for undetermined reasons, the excessive approach airspeed and the failure of the captain to align the airplane with the runway for the forced landing.

Aircraft Information

Registration
N7043G
Make
BEECH
Serial Number
LM-37
Engine Type
Turbo-shaft
Year Built
1967
Model / ICAO
65-A90-1BE9L
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
DYNAMIC AVLEASE INC
Address
PO BOX 7
Status
Deregistered
City
BRIDGEWATER
State / Zip Code
VA 22812-0007
Country
United States

Analysis

HISTORY OF FLIGHT

On June 12, 2006, about 1235 eastern daylight time, a Beech 65-A90-1 twin-engine, turboprop airplane, N7043G, registered to Dynamic AvLease, Inc., and operated by Dynamic Aviation Group, Inc., of Bridgewater, Virginia, contacted a taxiway then collided with a house during a forced landing at Peter O Knight Airport (TPF), Tampa, Florida. The flight was operating under the provisions of 14 Code of Federal Regulations (CFR) Part 91 as an other work use flight, and no flight plan was filed. Daylight marginal visual meteorological conditions prevailed in the area at the time of the accident for the local flight from Sarasota/Bradenton International Airport (SRQ), Sarasota, Florida. The airplane, house, and a vehicle parked there were destroyed by impact and a postcrash fire, and the captain was killed. The first officer/disperser (first officer) was seriously injured. The sole person in the house was not injured. The flight originated about 1130, from SRQ.

The purpose of the flight was to disperse sterile, Mediterranean fruit flies (fruit flies) under contract to the United States Department of Agriculture (USDA), and was scheduled to return to SRQ after dispersing was completed. The flight duration was estimated to be slightly over 1 hour.

The first officer reported that the mission dispersing the fruit flies was uneventful, and while returning to SRQ, "...we got a light on the panel for the [propeller] governor. Possibly for the right engine first." The captain began trouble shooting the right propeller annunciation issue by manipulating the power and propeller controls, and was trying to keep up with it as the right propeller was changing pitch. The same annunciation from the left propeller occurred approximately 1 minute after the annunciation for the right propeller. The captain asked him to pull a circuit breaker (CB) located immediately adjacent to his control yoke on the lower instrument panel, but he (first officer) could not recall if this occurred after the first or second annunciation. He also did not recall what CB he pulled, but he pulled the same CB two times at the request of the captain, which had no effect. The captain was manipulating the power and propeller controls for both engines following the left propeller annunciation, but he (first officer) did not think the captain's actions were having any effect. At some point the first officer noticed TPF was off their right wingtip and suggested to the captain to proceed there.

The captain advised him to contact air traffic control (ATC) and then to declare an emergency. At 1232:39, the first officer contacted Tampa Approach Control (Tampa Approach) and advised that they wanted to fly direct to TPF. The controller advised the flight crew to proceed direct to TPF and advise when the airport is in sight. Radar data indicated that, about this time, the airplane was at an altitude of about 1,200 feet mean sea level (msl) and was located about 3.2 nautical miles (nm) east-southeast from TPF, or approximately 8.5 nm southeast from Tampa International Airport. At 1232:54, the first officer declared an emergency with Tampa Approach, and requested a direct vector to TPF. The controller instructed the flight crew that the vector uncorrected for wind was 304 degrees and 3 miles, provided the altimeter setting, and gave the wind as being from 090 degrees at 7 knots. Radar data indicated that from 1232:54 (time first officer declared an emergency) to 1233:40, the flight proceeded in a northwesterly direction towards TPF and descended from 1,300 to 500 feet msl.

At 1233:50, the first officer reported to Tampa Approach that the airport was in sight. The radar data indicated that, about this time, the airplane was flying in a westerly direction at an altitude of about 500 feet msl, and was located south-southeast of the approach end of runway 35. The controller asked if they needed assistance, to which the first officer responded at 1233:57, "no we're just going to try to land." No further communications were received from the flight crew.

The first officer did not recall any conversation between himself and the captain while on approach to land at TPF. The captain did not advise him to extend the flaps or landing gear, and he did not recall extending either for landing. They were on a short right base for runway 35, and turned onto final approach but were not lined up with it due to the angle approaching the airport. Radar data indicated that from 1234:00 to 1234:13 (last radar target), the airplane descended from 400 to 100 feet msl, and the groundspeed at the last recorded radar target was 155 knots. The first officer was not sure how far abeam the runway they were, did not recall the approach airspeed, and believed both propellers were rotating. After landing it did not feel rough nor did he feel "multiple hits." The airplane began skidding and he knew they were unable to stop. The airplane collided with a fence, and after stopping, he asked the captain if he was OK but there was no response. He (first officer) exited the wreckage and rolled onto the ground to extinguish the fire. He was helped to a vehicle by a nearby person, and passed out in an ambulance. The next memory he had was approximately 10 days later.

Numerous witnesses at TPF reported the airplane was not lined up with the runway while on approach, the landing gear was retracted, and only one engine was operating. Two pilot-rated witnesses reported the wind at the airport at the time of the accident was from the south. One was based on a personal observation, and the other was based on the TPF automated weather observation system (AWOS), which indicated the wind was from 150 degrees at 4 knots.

A pilot-rated witness located at TPF stated that she heard a strange sounding engine directly above her. As she looked up, she saw the accident airplane flying "extremely fast" at about 200 feet above ground level (agl). The witness further stated that the airplane was observed between runways 35 and 03 flying in a northerly direction, and flew over runway 03. The airplane then banked to the left, and it appeared to her that the left wing contacted the ground just off taxiway "F," which is located west of runway 35. The airplane flew through a fence, hit a house, and immediately became engulfed in flames and exploded. She further reported there was no communication by the flight crew on TPF common traffic advisory frequency (CTAF).

Another pilot-rated witness who was located on the north side of the airport immediately adjacent to the accident site, stated the airplane flew towards him about 5 feet agl with the landing gear retracted and yawing to the right. While airborne, the airplane collided with a fence on the north border of the airport, and then collided with trees, a car, and finally a residence. The witness ran to the wreckage and assisted the first officer who exited via the airstair door. The first officer advised him the captain was on-board, but fire prevented the witness from rescuing him. The witness asked the first officer what occurred and he initially responded that they had lost one engine, proceeded towards TPF, then lost the second engine. They were able to restart one engine, and then the propeller governor "ran away on us." The witness further asked the first officer if they had run out of fuel and he reported no, one engine quit and he did not know why.

Local fire rescue responded and extinguished the fire.

PERSONNEL INFORMATION

The captain, age 41, was hired by Dynamic Aviation Group, Inc., on March 30, 2004, as base maintenance manager/first officer, and upgraded to captain on March 13, 2005. He held a commercial pilot certificate with ratings airplane single and multi-engine land, instrument airplane, issued October 15, 2003. The captain's most recent Federal Aviation Administration (FAA) first-class airman medical certificate was issued on April 1, 2006, and contained the limitation that, "Holder shall wear correcting lenses while exercising the [privileges] of his/her airman certificate." The captain indicated on his last medical certificate application that his total time was 2,120 hours.

Dynamic Aviation Group, Inc., records indicate that at the date the captain began employment, he did not have any Beech "King Air 90" flight time. His total flight time at that time was 1,519 hours, of which 1,058.9 hours were as pilot-in-command (PIC), and 213 hours in multi-engine airplanes. At the time of the accident, his total time was 1,907 hours, and his total PIC time was 1,451 hours. He had 457 hours total time and 305 hours as PIC in the accident make and model airplane, respectively. His last flight review in accordance with 14 CFR Part 61.56 occurred on March 13, 2005, when he upgraded to captain. At that time, he "Satisfactory" demonstrated knowledge of "Secondary Low Pitch Stop system failure."

The first officer, age 25, was hired by Dynamic Aviation Group, Inc., on May 3, 2006. He holds a commercial pilot certificate with ratings airplane single and multi-engine land, instrument airplane, issued December 15, 2004. His most recent first-class medical certificate with no limitations was issued on March 14, 2006.

Dynamic Aviation Group, Inc., records indicate that at the time the first officer began employment, he did not have any Beech "King Air 90" flight time. His total flight time at that time was 1,123 hours, of which 900 hours were as PIC, and 23 hours were in multi-engine airplanes. The first officer's pilot logbook indicates that at the time of the accident, he logged 44 hours total time in the accident make and model airplane; of which, 15 hours were logged as PIC. His last logged flight occurred on June 9, 2006; the flight was in the accident make and model airplane. Dynamic Aviation Group, Inc., personnel reported the first officer did not have any official flight training or ground based systems training since employment, but he (first of...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA06FA117