N70746

Substantial
None

Piper PA-32-300S/N: 32-40521

Accident Details

Date
Thursday, June 29, 2006
NTSB Number
DFW06LA172
Location
Midland, TX
Event ID
20060710X00904
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The partial loss of engine power as result of the maintenance personnel's failure to comply with a manufacture's Service Bulletin (SB). A contributing factor was the lack of suitable terrain for the forced landing.

Aircraft Information

Registration
N70746
Make
PIPER
Serial Number
32-40521
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
PA-32-300PA32
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
KENOBI JOE H
Address
3801 W 28TH ST APT 412A2
Status
Deregistered
City
LOS ANGELES
State / Zip Code
CA 90018-2385
Country
United States

Analysis

On June 29, 2006, about 1209 central daylight time, a Piper PA-32-300 single-engine airplane, N70746, was substantially damaged during an emergency landing following a partial loss of engine power near Midland, Texas. The non-instrument rated private pilot and passenger were not injured. The airplane was registered to and operated by the pilot. Visual meteorological conditions prevailed and no flight plan was filed for the 14 Code of Federal Regulations Part 91 personal flight. The 392-nautical mile cross-country flight originated at 1151 from the Midland Airpark (MDD) near Midland, Texas, and was destined for the Baytown Airport (HPY) near Baytown, Texas.

According to the 604-hour private pilot, approximately 14 minutes after she departed MDD, the engine started to "sputter." The pilot reported that she turned on the boost pump and switched fuel tanks; however, the engine continued to "sputter." Since she was unable to maintain altitude, the pilot elected to perform an emergency landing to a road. Shortly before the airplane touched down, the rotating beacon, which was located on top of the vertical stabilizer, collided with an unmarked static transmission line. During the landing roll the left wing tip impacted a mailbox.

A representative from the Federal Aviation Administration responded to the accident site and reported that the airplane's rudder had sustained structural damage.

An examination of the engine revealed that the right magneto's distributor gear bushing had failed. A review of the engine logbook revealed that the right magneto, a Teledyne Continental Motors (TCM) / Bendix S6LN-1200, P/N 10-349310-1, S/N H279705FR, had been installed on October 24, 1997, and had accumulated approximately 469 hours since it was last rebuilt.

According to Teledyne Continental Motors (TCM) service bulletin SB643B, section 3, paragraph C, a S-1200 "magneto must be overhauled or replaced at the expiration of five years since the date of original manufacture or last overhaul...without regard to accumulated operating hours."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW06LA172