Summary
On August 10, 2006, a Flight Design CTSW (N109CT) was involved in an incident near Hillsdale, MI. All 1 person aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's misjudged flare which resulted in the hard landing and his improper recovery from the bounced landing which resulted in the overload failure of the nose landing gear and subsequent nose over. The overload failure of the nose landing gear was a factor.
The light sport airplane was damaged during a hard landing. The pilot had just completed an hour of dual instruction in the accident airplane. He stated that during the accident he was sole occupant of the airplane. He stated that during the landing he touched down hard and bounced into the air. He stated that when the airplane touched down the second time the nose landing gear bent and the airplane went off of the left side of the runway. He stated that the bent nose landing gear became stuck in the grass and the airplane nosed over on its back. According to the pilot, the wind was from 40 degrees right of the runway heading at 4 to 6 knots.
This incident is documented in NTSB report CHI06CA226. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N109CT.
Accident Details
Probable Cause and Findings
The pilot's misjudged flare which resulted in the hard landing and his improper recovery from the bounced landing which resulted in the overload failure of the nose landing gear and subsequent nose over. The overload failure of the nose landing gear was a factor.
Aircraft Information
Registered Owner (Current)
Analysis
The light sport airplane was damaged during a hard landing. The pilot had just completed an hour of dual instruction in the accident airplane. He stated that during the accident he was sole occupant of the airplane. He stated that during the landing he touched down hard and bounced into the air. He stated that when the airplane touched down the second time the nose landing gear bent and the airplane went off of the left side of the runway. He stated that the bent nose landing gear became stuck in the grass and the airplane nosed over on its back. According to the pilot, the wind was from 40 degrees right of the runway heading at 4 to 6 knots.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI06CA226