N97949

Substantial
None

Stinson 108-1S/N: 108-949

Accident Details

Date
Monday, November 20, 2006
NTSB Number
LAX07LA040
Location
San Jose, CA
Event ID
20061124X01711
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Partial loss of engine power due to a seized exhaust valve during cruise flight. Rough terrain at the forced landing site was a contributing factor.

Aircraft Information

Registration
Make
STINSON
Serial Number
108-949
Engine Type
Reciprocating
Model / ICAO
108-1S108
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
108-1

Registered Owner (Current)

Name
FLINT RONNIE L
Address
PO BOX 215
City
FALLS CITY
State / Zip Code
NE 68355-0215
Country
United States

Analysis

On November 20, 2006, at 1238 Pacific standard time, a Stinson 108-1 airplane, N97949, lost engine power and nosed over during a forced landing near San Jose, California. The private pilot, who was the sole occupant, was not injured; the airplane sustained substantial damage. The pilot/owner operated the airplane under the provisions of 14 CFR Part 91 as a personal flight. Visual meteorological conditions prevailed and a flight plan was not filed. The local flight departed Reid-Hill View Airport (RHV), San Jose, California, at 1215.

According to the pilot, he was flying above hilly terrain southeast of the airport when he heard a loud bang, followed by a violent vibration coming from the engine. The pilot added that the engine did not experience a total loss of power, but performed poorly due to the severe vibration. The pilot reduced the throttle and the vibration subsided, but when he added more throttle the violent vibration returned. The pilot then decided that it was unsafe to continue the flight and began searching for a place to land. He made a forced landing in a pasture, which was uneventful until one of the main landing gear contacted a "deviation" in the ground. The airplane nosed over and came to rest inverted.

In a phone interview with the investigator-in-charge, a mechanic, who recovered the wreckage, reported that he examined the engine and discovered that the number 3 cylinder exhaust valve was stuck. The corresponding push rod tube was also bent, and the number 3 connecting rod was still intact.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# LAX07LA040