N9284P

Substantial
None

Piper PA-24-260BS/N: 24-4784

Accident Details

Date
Thursday, December 28, 2006
NTSB Number
CHI07LA056
Location
Belleville, IL
Event ID
20070129X00108
Coordinates
38.552776, -89.836112
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

The failure of the torque link bolt which resulted in the right main landing gear strut scissors separating and becoming jammed in the wheel well. Contributing to the accident was the seized torque link bolt due to surface corrosion.

Aircraft Information

Registration
Make
PIPER
Serial Number
24-4784
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
PA-24-260BPA24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
PA-24-260

Registered Owner (Current)

Name
DICKINSON MALCOLM
Address
69 AULDWOOD RD
City
STAMFORD
State / Zip Code
CT 06902-7815
Country
United States

Analysis

On December 28, 2006, at 1612 central standard time, a Piper PA-24-260B (Comanche), piloted by a commercial pilot, was substantially damaged while landing at Scott AFB/MidAmerica Airport (BLV), Belleville, Illinois. Visual meteorological conditions prevailed at the time of the accident. The personal flight was operating under the provisions of 14 Code of Federal Regulations (CFR) Part 91 without a flight plan. The pilot and his two passengers were not injured. The flight originated from Piatt County Airport (2K0), Monticello, Illinois, at 1507.

The pilot reported that after takeoff he selected landing gear-up, but the corresponding position light did not illuminate. He checked the landing gear motor circuit breaker and found it tripped. He selected landing gear-down and reset the circuit breaker. The landing gear did not fully extend, as indicated by the position of the emergency extension handle and the position lights. The pilot again attempted to retract the landing gear, but it only retracted about 90-percent before the landing gear motor circuit breaker tripped. The pilot decided to continue to BLV where he planned to perform an emergency landing gear extension prior to landing.

As the airplane neared BLV, the pilot attempted to lower the landing gear without success using the normal extension procedure. He then proceeded with the emergency landing gear extension procedure. The pilot was unable to get the landing gear to fully extend or retract during subsequent attempts. The control tower verified that the landing gear was not fully extended during a fly-by. The pilot decided to retract the landing gear as much as possible and perform a wheels-up landing in the grass area adjacent to runway 14. The airplane sustained substantial damage to a fuselage bulkhead during landing.

Inspection of the airplane showed that the left main and nose landing gear were completely retracted into their respective wheelwells. The right main landing gear was partially extended with its wheel and lower strut assembly rotated in the wheelwell. The AN174-13 bolt (p/n 402-313) that attached the upper and lower portions of the torque link assembly (p/n 20735-03) was sheared in half. The lower torque link was jammed against the wheelwell structure, which restricted the movement of the entire landing gear assembly.

The torque link assembly and bolt were sent to the National Transportation Safety Board's Materials Laboratory in Washington, D.C., for further examination. The bolt fracture features were consistent with shear overstress, as a result of torsion during the action of the torque link assembly. The bolt fracture face did not contain any evidence of fatigue cracking. The separated bolt sections were seized within the upper and lower torque links, as a result of surface corrosion.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI07LA056