N609PFCessna 180G2007-05-05 NTSB Accident Report

Substantial
None

Cessna 180GS/N: 18051328

Summary

On May 05, 2007, a Cessna 180G (N609PF) was involved in an incident near Lopez Island, WA. All 1 person aboard were uninjured. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's failure to maintain directional control during takeoff. Geese were a factor.

The pilot was conducting a Title 14, CFR Part 91 personal flight in a Cessna 180G airplane that nosed-over during takeoff. During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) shortly after the accident, the pilot stated that he was attempting to avoid geese on the private airstrip when the accident occurred. In a written report, dated May 26, 2007, the pilot stated "taxi down the runway - goose ran out in front - jammed on brakes and tailwind gust - flipped me over." The airplane sustained substantial damage to the empennage. The pilot did not report any preaccident mechanical anomalies. The pilot reported that his last medical, third class, was issued on October 21, 2003.

This incident is documented in NTSB report SEA07CA121. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N609PF.

Accident Details

Date
Saturday, May 5, 2007
NTSB Number
SEA07CA121
Location
Lopez Island, WA
Event ID
20070617X00756
Coordinates
48.483333, -122.933334
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's failure to maintain directional control during takeoff. Geese were a factor.

Aircraft Information

Registration
Make
CESSNA
Serial Number
18051328
Engine Type
Reciprocating
Model / ICAO
180GC180
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Analysis

The pilot was conducting a Title 14, CFR Part 91 personal flight in a Cessna 180G airplane that nosed-over during takeoff. During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) shortly after the accident, the pilot stated that he was attempting to avoid geese on the private airstrip when the accident occurred. In a written report, dated May 26, 2007, the pilot stated "taxi down the runway - goose ran out in front - jammed on brakes and tailwind gust - flipped me over." The airplane sustained substantial damage to the empennage. The pilot did not report any preaccident mechanical anomalies. The pilot reported that his last medical, third class, was issued on October 21, 2003. The medical carried a limitation that stated "not valid for any class after October 31, 2005."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# SEA07CA121