N704HF

Substantial
None

Cessna 150S/N: 15078618

Accident Details

Date
Saturday, March 24, 2007
NTSB Number
MIA07CA064
Location
Okeechobee, FL
Event ID
20070730X01038
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's failure to refuel the airplane prior to fuel exhaustion, which resulted in a loss of engine power during final approach, and a collision with a ditch.

Aircraft Information

Registration
Make
CESSNA
Serial Number
15078618
Engine Type
4-cycle
Model / ICAO
150C150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
150M

Registered Owner (Current)

Name
NO NAME AVIATION LLC
Address
108 W 13TH ST STE 105
City
WILMINGTON
State / Zip Code
DE 19801-1145
Country
United States

Analysis

The pilot stated that he completed a preflight and noted the airplane had 50 minutes worth of fuel. He arranged to have 4 more gallons of fuel added, which brought a total of 9.5 gallons of fuel onboard the airplane. He took a direct heading to Okeechobee after departure, cruising at 3,500 means sea level. The flight distance was about 51nactical miles with about 12 to 18 knots, northeast wind condition, giving an indication of 110 knots. He elected to land on runway 5 and was second to land, following another airplane in the downwind. During final, at about 250 feet above ground level, the airplane had a loss of engine power. He verified the engine controls; however, he had no time for an engine restart at the attitude the airplane was at. He elected to land on the grass prior to the runway. The airplane impacted with a 10 foot wide ditch about 255 feet from the runway's threshold and become airborne again. The nose gear bent and the bottom cowling was damaged before it came to a stop. He exited the airplane after securing the master switch and the magnetos. A gentleman from the airport came over with a tractor and assisted him in towing the airplane into a hanger. As the airplane was towed, he noticed fuel leaking from the airplane. He reached inside the cabin area and turned the fuel selector valve off. This was about 35-40 minutes after the incident occurred.

The person who assisted the pilot in recovery of the airplane from the accident site stated to the airport manager that he did not observe any fuel leaking from the airplane during the recovery process. He confirmed with the pilot that the fuel selector valve was in the off position before the airplane was moved. The FAA inspector that conducted the post accident examination of the airplane stated he drained 1.25 gallons of fuel from each wing tank. A total of 2.5 gallons of fuel was collected. The airplane's unusable fuel is 3.5 gallons as noted in the airplane's Type Certificate Data Sheet, 3A19.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# MIA07CA064