N16DK

Substantial
None

BEECHCRAFT 390S/N: RB-19

Accident Details

Date
Wednesday, February 13, 2008
NTSB Number
NYC08LA099
Location
Leesburg, VA
Event ID
20080310X00292
Coordinates
39.077777, -77.557502
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The airplane's runway excursion during landing roll following an encounter with ice. Contributing to the accident was the ice-covered runway, and the airport personnel's lack of knowledge regarding the runway condition.

Aircraft Information

Registration
N16DK
Make
BEECHCRAFT
Serial Number
RB-19
Engine Type
Turbo-jet
Model / ICAO
390PRM1
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
KEITH DENNIS E
Address
SKY RANCH 4260 S 1000 W POB 456
Status
Deregistered
City
HURRICANE
State / Zip Code
UT 84737
Country
United States

Analysis

HISTORY OF FLIGHT

On February 12, 2008, at 2055 eastern standard time, a Beechcraft Model 390 (Premier I), N16DK, was substantially damaged while landing at the Leesburg Executive Airport (JYO), Leesburg, Virginia. The certificated private pilot and passenger were not injured. Visual meteorological conditions prevailed and an instrument flight rules (IFR) flight plan was filed for the flight which originated at the Beech Factory Airport (BEC), Wichita, Kansas. The business flight was conducted under the provisions of 14 Code of Federal Regulations Part 91.

According to the pilot, he made a normal approach to runway 17 at JYO, and touched down at the "beginning" of the runway at an airspeed of 100 knots. As the airplane touched down on the runway, the braking was "adequate," and the airplane decelerated "normally." At approximately the mid-field point, the effectiveness of the braking decreased until it was "near nil," and the airplane was no longer decelerating.

The pilot maneuvered the airplane off the left side of the runway to gain traction from the grass located between the runway and the parallel taxiway. The airplane maintained its heading approximately parallel to the runway, until it came to a stop past the departure end of runway 17. After exiting the airplane, the pilot noticed the left main landing gear had collapsed, and the left wing was resting on the grass. He also stepped onto the departure end of the runway and observed the runway covered in black ice, with a thin layer of water.

The pilot reported no pre-impact malfunctions with the airplane.

PERSONNEL INFORMATION

The pilot held a private pilot certificate with ratings for airplane single-engine and multiengine land, instrument airplane, and rotorcraft-helicopter. He also held RA-390S and CE-525S type ratings. His most recent FAA second-class medical certificate was issued on December 6, 2007. At that time he reported 6,000 hours of flight experience.

AIRCRAFT INFORMATION

According to FAA records, the airplane was manufactured in 2001, and owned by the pilot. The airplane was a twin-engine airplane powered by two Williams FJ44 turbo-fan engines, and was not equipped with thrust reversers.

According to information provided by the aircraft manufacturer, and conditions applicable to the accident flight, the airplane flight manual (AFM), prescribed a Vref of 100 knots, with a required landing distance on an uncontaminated runway of approximately 2,714 feet.

The Airplane Flight Manual (AFM) Contaminated Runway Supplement stated "operations on runways contaminated with ice or wet ice are not recommended. A runway is considered as wet when there is sufficient moisture on the surface to cause it to appear reflective, but without significant areas of standing water." Using the supplement, the anticipated landing distance on a wet runway was calculated to be 3,343 feet.

According to the Aeronautical Information Manual Pilot/Controller Glossary, a runway, "is considered contaminated whenever standing water, ice, snow, slush, frost in any form, heavy rubber or other substances are present."

METEOROLOGICAL INFORMATION

Weather reported at JYO, at 2100, included calm wind, 5 miles visibility with light snow, overcast clouds at 1,100 feet, temperature -2 degrees Celsius (C), dew point -3 degrees C, and altimeter setting of 30.06 inches of mercury.

Weather reported at Dulles International Airport (IAD), 10 miles to the southeast, at 2052, included wind from 050 degrees at 4 knots, 10 miles visibility, a broken cloud layer at 20,000 feet, temperature 4 degrees C, dew point -3 degrees C, and altimeter setting of 30.15 inches of mercury.

AIRPORT INFORMATION

Leesburg Executive Airport was comprised of a single runway oriented in a 17/35 configuration. Runway 17 was a 5,500-foot-long and 100-foot wide, asphalt runway.

An employee of the fixed base operator (FBO) at the airport reported that at the time of the accident the main ramp and taxiways were coated with 1/4 to 1/2 inch of ice from earlier precipitation. The last aircraft to land prior to N16DK, was a Lear 40 that landed at 1820, uneventfully.

The airport manager reported at 1730, when he was leaving for the day, the forecast was for little or no precipitation and the temperature was expected to increase. However, the temperature decreased instead, resulting in the formation of ice on the runway. The airport manager reported at the time of the accident the north end of runway 17 was dry; however, the south end of runway 17 had "some ice on it."

The normal procedure for the airport to treat ice on the runway was to issue a NOTAM to close the runway and deploy their ice melt product. Then, they would cancel the NOTAM and issue another one stating that ice is present on the runway. Because the temperature was forecast to rise and not fall, the airport did not use any ice melt product on the runway.

The airport personnel did not have the equipment or training to issue braking action reports, nor was it required.

WRECKAGE AND IMPACT INFORMATION

Examination of the airplane by a representative of the manufacturer revealed the left main landing gear punctured the wing, resulting in substantial damage to the wing. No preimpact mechanical deficiencies were identified.

Additionally, examination of the runway environment by a Federal Aviation Administration inspector revealed the airplane impacted a drainage ditch as it exited the left side of runway 17, which caused the damage to the airplane. The inspector reported the area off the end of runway 17 was an open field with no obstructions.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC08LA099