N9639G

Substantial
None

CESSNA A188BS/N: 18801575

Accident Details

Date
Thursday, June 12, 2008
NTSB Number
DEN08LA103
Location
Lyons, KS
Event ID
20080624X00896
Coordinates
38.342777, -98.226669
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

the loss of engine power for undetermined reasons. A contributing factor was the dirt embankment.

Aircraft Information

Registration
N9639G
Make
CESSNA
Serial Number
18801575
Engine Type
Reciprocating
Year Built
1974
Model / ICAO
A188BC188
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
J & C ENTERPRISES AVIATION INC
Address
14 AIRPORT RD
Status
Deregistered
City
THOMAS
State / Zip Code
OK 73669-7400
Country
United States

Analysis

On June 12, 2008, approximately 1400 central daylight time, a Cessna A188B single-engine agricultural airplane, N9639G, sustained substantial damage when it impact terrain during a forced landing following a loss of engine power near Lyons, Kansas. The airline transport pilot, who was the sole occupant, was not injured. The airplane was registered to Ellinwood Flying Service, Inc., Ellinwood, Kansas, and operated by Rice County Aerial Sprayers, Lyons, Kansas. Visual meteorological conditions prevailed, and a flight plan was not filed for the Title 14 Code of Federal Regulations Part 137 aerial application flight. The local flight was originating at the time of the accident.

According to the pilot, on May 26, 2008, he experienced an engine problem during an attempted aerial application flight, and landed successfully in an open field near the Lyons airport. After maintenance was performed which included new spark plugs, and checking the fuel and oil systems; the airplane underwent several engine test runs and a couple of test flights with no problems noted.

On the day of the accident, the airplane was loaded with approximately 150 gallons of chemical. After takeoff, the pilot turned the airplane in a direction opposite of his intended destination in order to over fly the airport in case of an emergency. During the initial takeoff climb, the engine was running okay and no problems were noted. Approximately 1 to 1.5 miles from the airport, the engine "pulled down," and the pilot could not maintain altitude. The pilot stated, "I am now sure the engine was trying to seize up and I was again forced to land." The pilot elected to perform a forced landing to a field. During the forced landing, the airplane impacted a dirt embankment, went onto its nose, and came to rest upright.

In 2002, the Continental IO-520-D engine underwent a major overhaul. At the time of the accident, the engine had accumulated approximately 600 hours since major overhaul. The engine underwent its most recent 100-hour inspection on January 15, 2008. Examination of the engine by a Federal Aviation Administration airworthiness inspector revealed no anomalies. The oil filter and oil screens were clear of debris. The reason for the loss of engine power was not determined.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DEN08LA103