Accident Details
Probable Cause and Findings
A partial loss of engine power due to fuel starvation. Contributing to the accident was the pilot’s decision to add only a limited amount of fuel prior to the flight, and the fuel selector valve placards' inaccurate depiction of the airplane fuel tank configuration.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On July 22, 2008, about 1350 eastern daylight time, a Cessna 402B, N3990C, was substantially damaged when it impacted a building and the ground in Ocean Ridge, Florida. The certificated commercial pilot, the sole occupant, was seriously injured. The personal flight was operated under the provisions of Title 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed for the flight, and no flight plan was filed.
The pilot stated that the purpose of the flight was to reposition the airplane from Palm Beach County Park Airport (LNA), West Palm Beach, Florida, to Pompano Beach Airpark (PMP), Pompano Beach, Florida, for future maintenance. PMP was located approximately 22 miles south of LNA. Statements provided by line personnel at LNA indicated that the pilot purchased 20 gallons of fuel just prior to the accident flight, and that the fuel was dispensed evenly into the two tip tanks of the accident airplane.
In interviews with Federal Aviation Administration (FAA) inspectors, the pilot stated that he took off from LNA and kept the airplane’s landing gear extended for the flight. He was aware of a problem with the landing gear, and thought that if he retracted the gear, he would not be able to successfully re-extend it for landing. After departing LNA, the pilot flew south over the Atlantic Intracoastal Waterway at an altitude of between 800 and 1,000 feet, enroute to PMP.
The pilot reported that about 5 minutes into the flight, he experienced a "loss of engine power." In one interview with FAA inspectors, he stated that he had problems with the left engine, but during a subsequent interview, he stated that the right engine malfunctioned. In a written statement that the pilot provided to the Ocean Ridge Police Department, dated 6 days after the accident, the pilot did not specify which engine malfunctioned. Instead, he reported only that he attempted to "identify and verify which engine(s) were causing trouble." In the same statement, the pilot reported that he started to lose altitude "rapidly," and attempted to "wag the wings" side to side in order to "get all the fuel to be useable." He stated that he "must have blanked out," because the last thing he remembered about the accident was seeing the top of the town hall building just prior to impact. The airplane struck the Ocean Ridge town hall building, located approximately 8 miles south of LNA.
Several witnesses reported that the airplane was traveling north to south, was flying slowly with the landing gear extended, and that the wings were "rocking." Many witnesses also reported that the engines were operating.
PERSONNEL INFORMATION
According to FAA records, the pilot, age 50, held a commercial pilot certificate with airplane single-engine land, multi-engine land, and instrument ratings. In 2004, the pilot reported that he had 1,560 total hours of flight experience. His most recent FAA second-class medical certificate was issued in February, 2008. Despite multiple requests, the pilot did not provide his personal logbook or other information requested by National Transportation Safety Board (NTSB).
AIRCRAFT INFORMATION
The accident airplane was an all-metal, twin-engine, low-wing monoplane, with retractable landing gear. According to FAA records, the airplane was manufactured in 1975. It was powered by two Continental TSIO-520 series engines, each equipped with a three-bladed, constant-speed propeller. The airplane was previously owned by the pilot, but he sold it to another individual in September 2007, and the FAA airplane registration form was issued to that individual in January, 2008. The individual who owned the airplane at the time of the accident did not hold any pilot certificates.
METEOROLOGICAL INFORMATION
The 1347 surface weather observation at an airport located 6 miles south of the accident site included winds from 160 degrees at 8 knots, visibility 10 miles, scattered clouds at 2,500 feet, temperature 30 degrees C, dew point 25 degrees C, and an altimeter setting of 30.08 inches of mercury.
COMMUNICATIONS
No air traffic control voice communications or ground radar tracking data regarding this flight were able to be located.
WRECKAGE AND IMPACT INFORMATION
After it struck the building, most of the airplane came to rest inverted on the ground, against a concrete utility pole. There was no post-impact fire. The left wing was separated from the fuselage, and the left tip tank was separated from the left wing. The right wing and fuselage were on opposite sides of a concrete utility pole, and were structurally separated from one another, but remained attached by wires and control cables. The outboard section of the right wing, including the tip tank, was separated from the inboard wing. The fuselage was fractured just aft of the pilots' seats. The horizontal stabilizer was separated from the fuselage. The left engine was found approximately 25 feet from the main wreckage, and the left propeller was separated from the left engine. The right engine remained attached to the airframe, and the right propeller remained attached to the right engine. All three landing gear were found in their respective down and locked positions. The left landing gear, left engine nacelle and a portion of the left inboard wing were found on the roof of the building.
ADDITIONAL INFORMATION
Maintenance Records Examination
A review of the airframe and engine maintenance records that dated back to February 2002 revealed that only three annual inspections were recorded over the 6 year period.
An annual inspection was completed in February 2002, when the airplane had accrued a total time (TT) in service of 7,135 hours. The corresponding Hobbs meter entry in each engine logbook (only one Hobbs meter was installed in the airplane) indicated that each engine had accrued 856.2 hours since major overhaul (SMOH). The next annual inspection was completed in March 2004, when the airplane had accrued a TT of 7,145.8 hours, and the Hobbs meter reading was recorded as 866.4 hours. The most recent annual inspection was completed in March 2006, when the airplane had accrued a TT of 7,221.9 hours, and the Hobbs meter reading was recorded as 942.5 hours. The March 2006 annual inspection was the most recent entry in the airframe, engine and propeller maintenance records.
Detailed Airframe Examinations
Recovery personnel had separated the fuselage into two pieces, and they had also detached the right wing. On August 5, 2008, personnel from the FAA, Cessna Aircraft, and Teledyne Continental Motors (TCM) and the NTSB examined the airplane at the recovery facility in Boynton Beach, Florida. On March 10, 2010, NTSB personnel re-examined selected portions of the fuel system.
The cockpit area and instrument panel were relatively intact, with some crush and deformation damage. The cockpit throttle, propeller, and mixture controls were all found at or near their full-forward positions. The two magneto switches for the left engine, and the left magneto switch for the right engine, were in their respective "On" positions. The right magneto switch for the right engine was in the "Off" position. The "L Alt" and "Batt" master switches were in their respective "On" positions, and the "R Alt" master switch was in the "Off" position. The two guarded emergency power switches were found in different positions. The "Alt Field" cover was down (stowed), while the "Avionics Bus" cover was up, with its switch in the up/forward position. Numerous circuit breakers on the left side circuit breaker panel, including "Turn & Bank 1, L Fuel Pump, Comm 3, ADF, DME, Audio Amp, Xpndr 1, and Radar" were in the activated (circuit disabled) position. The Hobbs hour meter in the cockpit indicated 969.1 hours, and a placard below it stated "Total Time Add 6279.4 Hrs."
The landing gear handle was found in the gear-retracted position, but the positions or configurations of most other landing gear linkage and components, including the gearbox, were consistent with the landing gear in the extended position.
All flight control surfaces were present, and control continuity was established for all primary and secondary flight controls. The elevator trim indicator in the cockpit was found at the extreme airplane-nose-down position. The elevator trim actuator extension was 1.9 inches, which was beyond its normal travel limit, in a tab-up (airplane-nose-down) direction. The aileron trim indicator in the cockpit was found in the right-wing-down position. The left wing aileron trim actuator extension was 1.9 inches, which equated to approximately 15 degrees tab down, and which would result in a left-wing-down rolling moment. The rudder trim indicator in the cockpit was found in the airplane-nose-left position. The rudder trim actuator extension was 2.3 inches, which equated to a neutral (zero degrees) tab deflection. The cockpit flap selector handle was positioned to 30 degrees, and the flap deflection indicator was positioned between the 0 and 15 degree deflection markings. The extension of the flap hydraulic actuator was deemed to be unreliable for the purpose of determining flap position.
All three blades remained in the right propeller hub. Two blades appeared undamaged, and one blade was bent slightly aft. The spinner sustained some crush damage in the aft direction, with straight scoring in the fore-aft direction. The left propeller hub was fractured, and one blade had separated from the hub. The separated blade exhibited spanwise scoring and some aft bending. One blade that remained in the hub was bent slightly aft, and the other blade in the hub exhibited significant "S" bending, with moderate chordwise and spanwise scoring.
Airplane Fuel System Configuration and Examination
The airplane was equipped with four fuel tanks, including one main (tip) tank, and one auxiliary tank, in each wing. According to Cessna records, the airplane was delivered new with two main f...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC08LA255