N45133

Substantial
Minor

CESSNA 177RGS/N: 177RG1094

Accident Details

Date
Sunday, June 8, 2008
NTSB Number
NYC08CA208
Location
Bessemer, AL
Event ID
20081003X17821
Coordinates
33.312500, -86.926109
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

Failure of the left magneto for undetermined reasons resulting in a partial loss of engine power during takeoff.

Aircraft Information

Registration
N45133
Make
CESSNA
Serial Number
177RG1094
Engine Type
Reciprocating
Year Built
1976
Model / ICAO
177RGC77R
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BEST HARLAN W
Address
5540 OAK ST
Status
Deregistered
City
MC CALLA
State / Zip Code
AL 35111-3237
Country
United States

Analysis

According to one of the pilots of the Cessna 177RG, during the preflight inspection, he observed approximately 35 gallons of fuel onboard. The other pilot sumped the fuel tanks and no water was present. After engine start, runup was "normal," and the pilots completed the pre-takeoff checklists with no anomalies noted. After takeoff, the pilot at the controls retracted the landing gear and "immediately" observed a "very noticeable" drop in rpm and airspeed. With insufficient runway remaining, he made a slight turn to avoid obstacles at the end of the runway, lowered the landing gear, extended the flaps, and reduced power. The airplane impacted terrain, bounced back into the air, and impacted trees. The airplane came to rest nose-down at the base of a tree. The pilots exited the airplane, and because of a strong odor of fuel, turned the fuel selector to the "off" position, and turned off the master switch. Neither the pilots nor the on-scene Federal Aviation Administration inspector reported any mechanical anomalies on scene. The inspector also confirmed cylinder compression and spark from the dual magnetos. The airplane was subsequently moved to a salvage yard, where an engine run was performed under Safety Board oversight. The engine started after 5 to 6 turns, and ran for about 5 minutes. During magneto checks, the left magneto of the dual magneto appeared to be operating abnormally, resulting in increased engine shaking as the rpm was increased. The engine ran normally on the right magneto.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# NYC08CA208