N5471Q

Substantial
None

CESSNA 150LS/N: 15073371

Accident Details

Date
Friday, June 13, 2008
NTSB Number
CHI08LA162
Location
Summerville, SC
Event ID
20081004X12023
Coordinates
33.049369, -80.189628
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A total loss of engine power for undetermined reasons.

Aircraft Information

Registration
Make
CESSNA
Serial Number
15073371
Engine Type
Reciprocating
Year Built
1972
Model / ICAO
150LC150
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
150L

Registered Owner (Current)

Name
GUNNARSSON JON
Address
8064 RONALD AVE
City
CONCRETE
State / Zip Code
WA 98237-9271
Country
United States

Analysis

On June 13, 2008, approximately 1930 eastern daylight time, a Cessna 150; N5471Q, operated and piloted by a commercial pilot crashed shortly after takeoff from Summerville Airport, Summerville, South Carolina. Visual meteorological conditions prevailed at the time of the accident and the flight was was being conducted as a ferry flight under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91 without a flight plan. The pilot, the only occupant, was not injured during the accident. The local flight was originating for the purpose of ferrying the aircraft about 25 miles to Mt Pleasant Regional Airport-Faison Field (KLRO).

The pilot said the engine originally started without hesitation and he taxied to runway 24 for takeoff. Upon reaching the runway, the run up indicated there was a fouled plug in the engine. Several minutes were spent clearing up the fouled plug and the pilot proceeded to takeoff. He reported he had 2475 rpm on takeoff, but, passing though about 60 feet above the ground after takeoff, the engine suddenly stopped producing power. Manipulating the throttle caused a momentary return of power, but, the engine stopped again so the pilot made a forced landing straight ahead.

A Federal Aviation Inspector inspected the engine and found the magnetos would spark and there was compression in all cylinders. The inspector also disassembled the carburetor and found no anomalies with the carburetor.

The pilot submitted a written statement but not an aircraft accident report.

The airplane and engine both had current annual inspections. The engine had 1800 hours since major overhaul.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CHI08LA162