Summary
On July 17, 2008, a Piper PA-30 (N44HM) was involved in an incident near Rockport, TX. All 3 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's failure to complete all cockpit checklist items prior to takeoff. Contributing to the accident was the pilot's failure to properly configure the landing gear switch.
The pilot was on the takeoff roll at approximately 90 knots when he took his hands off the throttles and began applying back pressure for liftoff. Almost immediately the aircraft began to sink, followed by the sounds of the props striking the runway. All three landing gear were partially retracted as the airplane slid along the runway surface and came to a stop with resulting substantial damage to the belly structure. The pilot and both passengers were not injured. After the accident, the pilot discovered that he had inadvertently left the landing gear switch in the "up" position while completing other items in the cockpit checklist. During the recovery operations the airplane was then jacked and the gear was lowered normally.
This incident is documented in NTSB report DFW08CA193. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N44HM.
Accident Details
Probable Cause and Findings
The pilot's failure to complete all cockpit checklist items prior to takeoff. Contributing to the accident was the pilot's failure to properly configure the landing gear switch.
Aircraft Information
Registered Owner (Historical)
Analysis
The pilot was on the takeoff roll at approximately 90 knots when he took his hands off the throttles and began applying back pressure for liftoff. Almost immediately the aircraft began to sink, followed by the sounds of the props striking the runway. All three landing gear were partially retracted as the airplane slid along the runway surface and came to a stop with resulting substantial damage to the belly structure. The pilot and both passengers were not injured. After the accident, the pilot discovered that he had inadvertently left the landing gear switch in the "up" position while completing other items in the cockpit checklist. During the recovery operations the airplane was then jacked and the gear was lowered normally.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DFW08CA193