N620KJD-Fly UL Stork2009-01-31 NTSB Accident Report

Substantial
None

D-Fly UL StorkS/N: 002

Summary

On January 31, 2009, a D-fly UL Stork (N620KJ) was involved in an incident near Jackson, GA. All 1 person aboard were uninjured. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's inadvertent activation of an engine cutoff switch during cruise flight.

The pilot/owner of an experimental, amateur built, UL Stork was in cruise flight at 1,500 ft agl, when he shut down the engine by inadvertently activating a recently installed, unguarded, engine cutoff switch located on the control stick. After two unsuccessful attempts to restart the engine, he performed an off field landing to a golf course. During the landing roll the airplane impacted a metal box resulting in damage to the landing gear, propeller, and left wing strut.

This incident is documented in NTSB report ERA09CA149. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N620KJ.

Accident Details

Date
Saturday, January 31, 2009
NTSB Number
ERA09CA149
Location
Jackson, GA
Event ID
20090201X10705
Coordinates
33.319999, -83.942497
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's inadvertent activation of an engine cutoff switch during cruise flight.

Aircraft Information

Registration
Make
D-FLY
Serial Number
002
Engine Type
Reciprocating
Model / ICAO
UL StorkWLBY
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
UL STORK

Registered Owner (Current)

Name
MAY JOHN D
Address
435 ANGEL DR
City
AUSTIN
State / Zip Code
AR 72007-8861
Country
United States

Analysis

The pilot/owner of an experimental, amateur built, UL Stork was in cruise flight at 1,500 ft agl, when he shut down the engine by inadvertently activating a recently installed, unguarded, engine cutoff switch located on the control stick. After two unsuccessful attempts to restart the engine, he performed an off field landing to a golf course. During the landing roll the airplane impacted a metal box resulting in damage to the landing gear, propeller, and left wing strut.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA09CA149