N9348S

Substantial
None

BEECH B24RS/N: MC-350

Accident Details

Date
Sunday, March 15, 2009
NTSB Number
CEN09LA209
Location
Bellefontaine, OH
Event ID
20090316X92527
Coordinates
40.372222, -83.819999
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The inadequate torque of the Number 3 cylinder rod bolts by maintenance personnel, which resulted in a failure of the connecting rod and a total loss of engine power.

Aircraft Information

Registration
N9348S
Make
BEECH
Serial Number
MC-350
Engine Type
Reciprocating
Year Built
1975
Model / ICAO
B24RBE24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MIERZEJEWSKI KEVIN A
Address
1665 PEVEE RD
Status
Deregistered
City
ADA
State / Zip Code
OH 45810-9211
Country
United States

Analysis

On March 15, 2009, at 1500 eastern daylight time (edt), a Beech B24R (Sierra), N9348S, owned and piloted by a private pilot, was substantially damaged during a forced landing following an en route loss of engine power near Bellefontaine, Ohio. Visual meteorological conditions prevailed at the time of the accident. The personal flight was operating under the provisions of 14 Code of Federal Regulations (CFR) Part 91 without a flight plan. The pilot and his passenger were not injured. The flight departed Grimes Field Airport (I74), near Urbana, Ohio, at 1445 edt and was en route to Bluffton Airport (5G7), near Bluffton, Ohio.

According to the pilot, the airplane was in cruise flight when he noticed abnormal engine noises and a partial loss of engine oil pressure. He immediately diverted to the nearest airport, Bellefontaine Regional Airport (KEDJ), and entered downwind for runway 7 (4,999 feet by 100 feet, asphalt). During the turn to base leg, the engine oil pressure dropped to zero pounds per square inch and the engine seized. He established best glide speed and continued the turn onto final approach. The pilot reported that the airplane was not in a position to reach the runway threshold, or to clear the airport perimeter fence. He lowered the landing gear and selected full flaps prior to landing in the grass area outside of the airport perimeter fence. During landing rollout the airplane impacted the airport perimeter fence, damaging both wings and the nose landing gear.

An engine teardown examination revealed that the number 3 cylinder connecting rod assembly had separated from its corresponding crankshaft journal. The crankshaft journal surface was blue in color, consistent with exposure to excessive heat and lack of lubricant. The oil suction screen was obstructed with bearing material. The number 3 cylinder connecting rod cap was found jammed beneath the counterbalance weight. One of the two connecting rod stretch bolts remained intact. The corresponding nut was found finger tight. The measured torque for the upper and lower stretch bolts on the number 2 cylinder connecting rod was 15 foot-pounds (ft-lbs) and 6 ft-lbs, respectively. The manufacturer specified torque value was 40 ft-lbs. The Lycoming IO-360-A1B6 engine, serial number L-13455-51A, had accumulated 492.7 hours since its last overhaul in September 1999 following a propeller strike.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN09LA209