N708RW

MINR
None

Cirrus Design Corporation SR22S/N: 5140

Accident Details

Date
Friday, July 3, 2009
NTSB Number
CEN09IA438
Location
Put-In-Bay, OH
Event ID
20090714X71423
Coordinates
41.639976, -82.819107
Aircraft Damage
MINR
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's failure to maintain directional control while landing with a crosswind.

Aircraft Information

Registration
Make
CIRRUS DESIGN CORPORATION
Serial Number
5140
Engine Type
Reciprocating
Year Built
2003
Model / ICAO
SR22SR22
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
SR22

Registered Owner (Current)

Name
BANKS WES J
Address
1530 E F ST
City
OAKDALE
State / Zip Code
CA 95361-9611
Country
United States

Analysis

On July 3, 2009, at 1810 eastern daylight time, a Cirrus Design Corporation, SR22, N708RW, received minor damage when it veered off the runway and impacted terrain during landing at Put-In-Bay Airport (3W2), Put-In-Bay, Ohio. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 flight was not operating on a flight plan. The pilot and passenger were uninjured. The flight last departed from Akron Fulton International Airport, Akron, Ohio, at 1630.

According to a police report, an officer of the Put-In-Bay Police Department contacted the pilot on July 6, 2009. The pilot stated to the officer that a "big gust" of wind blew the airplane off the runway. The pilot would not give the officer any further information pertaining to him or to the incident.

The pilot stated that during the approach to runway 21 (2,870 feet by 75 feet, asphalt), which had a displaced threshold of 657 feet, he performed a go-around after a report of wind conditions by a preceding airplane. During the second landing attempt, the airplane reportedly experienced wind sheer and turbulence that "pushed" the airplane off the runway where it rolled into the grass and at one point the propeller "touched" the ground. The pilot taxied the airplane back onto the runway and parked the airplane.

The airplane's short final approach ground speed was approximately 82 knots. After touchdown, the airplane departed the left side and traversed the area adjacent to the runway. The airplane ground speed was approximately 78 knots abeam the center of the runway and decelerated to approximately 8 knots where the airplane then crossed over the departure end of the runway. The airplane then taxied along the taxiway to the airplane parking area.

According to a Federal Aviation Administration inspector, the pilot taxied the airplane through rocks at high speed, and upon exiting the rock area, the propeller struck the ground/rocks. The pilot then proceeded to taxi through a drainage ditch where the propeller struck the ground/ditch multiple times while exiting the ditch.

The airplane propeller and landing gear wheel fairings were damaged.

Post accident inspection of the airplane revealed no anomalies that would have precluded normal operation.

The pilot's airman medical certificate was expired at the time of the incident.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN09IA438