N6140S

Substantial
Minor

BROWN MICHAEL KITFOX IVS/N: C9909-0253

Accident Details

Date
Saturday, July 25, 2009
NTSB Number
WPR09LA369
Location
Escondido, CA
Event ID
20090726X30611
Coordinates
33.152778, -116.906944
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of power due to an oil exhaustion induced seizure of the engine. The pilot's decision to continue flight to the original destination after becoming aware of the in-flight oil leak instead of landing at an intermediate airport to investigate the source and extent of the problem is also causal. Contributing to the accident was the pilot's reuse of the pushrod oil seal during maintenance in contradiction to the engine manufacturer's maintenance instructions.

Aircraft Information

Registration
Make
BROWN MICHAEL
Serial Number
C9909-0253
Engine Type
Reciprocating
Year Built
2001
Model / ICAO
KITFOX IVFK9
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
KITFOX IV

Registered Owner (Current)

Name
SZYLOBRYT JONATHAN A
Address
264 TUSHER ST
City
MOAB
State / Zip Code
UT 84532-2738
Country
United States

Analysis

HISTORY OF FLIGHT

On July 25, 2009, about 1100 Pacific daylight time, an experimental Kitfox IV, N6140S, nosed over after a forced landing near Escondido, California. The pilot/owner was operating the airplane under the provisions of 14 Code of Federal Regulations Part 91. The certificated sport pilot received minor injuries. The airplane sustained substantial damage to the aft fuselage and vertical stabilizer. The personal flight departed Hemet, California, about 1030, with a planned destination of Ramona Airport, Ramona, California. Visual meteorological conditions prevailed, and no flight plan had been filed.

After departing Hemet, and as the airplane approached Pauma Valley Airpark (CL33), Pauma Valley, California, the pilot observed oil trailing along the left landing gear strut. He checked the engine oil pressure indicator, and confirmed it was displaying 45 to 50 pounds per square inch (PSI). He elected to continue the flight to Ramona; however, he altered his course so that he was able to fly over several areas, including a private ranch landing strip, where a landing could be made if it was necessary. He reported that as he approached the private landing strip the oil pressure did not change, and he decided to continue the flight to Ramona.

After flying for an additional 2 miles, he observed the oil pressure level drop to zero, and shortly thereafter, the engine stopped. He then changed his heading to the north, and prepared for a forced landing. The airplane landed in a dirt field. During the landing roll the main landing gear struck a ditch, and the airplane nosed over.

The pilot reported performing a preflight inspection on a prior flight earlier in the day. During the inspection he confirmed that the engine contained adequate oil. He stated that on the accident flight, he had not checked the engine oil level.

AIRCRAFT INFORMATION

The two-seat, experimental airplane, was issued a Special Airworthiness Certificate in December 2001. It was powered by a four-cylinder, liquid cooled, Rotax 912 ULS engine, and equipped with a Sensenich ground adjustable composite propeller. The engine incorporated a dry sump forced lubrication system with an oil tank capacity of 3.2 quarts.

The engine was manufactured in 2001; 330.3 flight hours prior to the accident. Maintenance records revealed that an annual inspection was completed on June 1, 2009; 8.2 flight hours prior to the accident.

TESTS AND RESEARCH

Engine

The NTSB investigator-in-charge and representatives from the Federal Aviation Administration and Rotax Aircraft Engines examined the engine.

The engine could not be rotated by hand. Removal of the engine oil dipstick, and visual inspection of the oil tank revealed the absence of oil. Oil streaks were observed on the left main landing gear strut, with the left side of the belly mounted engine coolant radiator oil soaked. External inspection of the engine revealed no obvious sources of an oil leak.

Investigators connected a 15 PSI regulated air source to the engine oil tank breather line, and observed air leaking from the base of the number four cylinder exhaust pushrod. Removal of the cylinder revealed the exhaust pushrod O-ring seal had spilt.

The pilot/owner stated that about 2 years, and 100 flight hours prior to the accident, he had removed the number four cylinder head in order to perform a repair of the spark plug hole. He stated that he reused the original O-ring seal during reassembly of the cylinder head.

In the 'Procedure Notes' section of the 912 Series Rotax Engine Maintenance Manual it states, "At reassembly of the engine, replace all sealing rings, gaskets, securing elements, O-ring and oil seals."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR09LA369