N9368G

Substantial
None

CESSNA A188BS/N: 18801460

Accident Details

Date
Sunday, November 8, 2009
NTSB Number
ERA10LA059
Location
Ripley, MS
Event ID
20091110X35259
Coordinates
34.722221, -89.014999
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot’s failure to maintain adequate airspeed on final approach, which resulted in an aerodynamic stall. Contributing to the accident was a partial loss of engine power due to water in the fuel.

Aircraft Information

Registration
N9368G
Make
CESSNA
Serial Number
18801460
Engine Type
Reciprocating
Year Built
1973
Model / ICAO
A188BC188
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WOOLIE ENTERPRISES INC
Address
401 LAKEVIEW DR
Status
Deregistered
City
OLDSMAR
State / Zip Code
FL 34677-4505
Country
United States

Analysis

On November 8, 2009, about 1000 central standard time, a Cessna A188B, N9368G, was substantially damaged during a forced landing while on final approach to Ripley Airport (25M), Ripley, Mississippi. The certificated private pilot was not injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the local personal flight, which was conducted under the provisions of 14 Code of Federal Regulations Part 91.

According to the pilot, he performed a preflight inspection of the airplane before starting the engine and letting it warm up for about 5 minutes. He then back-taxied on runway 3, and performed the run-up checklist before taking off. He subsequently flew the traffic pattern and was on final approach, at an altitude of about 500 feet, when the engine lost power about 250 feet from the end of the runway. The airplane then “went into a right hand dive and hit the ground.”

One witness, who was sitting on his sofa in his house, heard the airplane “sputter and pop loudly.” After that, he “did not hear the engine and assumed the plane went down.” When he went outside, he “saw the airplane sitting adjacent to [his] house.”

Another witness was in a field when he saw the airplane fly over, “and heard the plane sputtering and cutting out.” When he spoke to the pilot, the pilot stated that “the engine had lost power.”

According to a Federal Aviation Administration (FAA) inspector, an on-scene examination of the airplane revealed that the right wing and the engine were separated from the airplane, that there was no fuel in the left wing tank, and that the little fuel that could be found was contaminated with water.

According to a sheriff’s department report, the responding officer noted that fuel was “leaking…from the wing and was on the ground” when he arrived.

Accident photographs revealed that one of the two propeller blades was almost straight, but exhibited chordwise scratching, significant leading edge burnishing in one area, and curling at the blade tip with part of the tip torn off. The other propeller blade exhibited chordwise scratching, some s-bending along most of its length, and severe s-bending and curling at the blade tip.

The FAA inspector noted that due to the pilot relinquishing his certificate, no further examination of the airplane was conducted.

The pilot, age 43, held a private pilot certificate with a single engine land rating, and reported 394 hours of total flight time.

Winds, recorded at an airport 29 nautical miles southeast of the accident site, at 1001, were from 060 degrees true, at 11 knots.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA10LA059