N5065X

Substantial
None

American Champion 7KCABS/N: 147

Accident Details

Date
Tuesday, February 23, 2010
NTSB Number
CEN10LA198
Location
Greeley, CO
Event ID
20100410X23336
Coordinates
40.419166, -104.633331
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

An in-flight failure of the wing fabric for undetermined reasons.

Aircraft Information

Registration
Make
AMERICAN CHAMPION
Serial Number
147
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
7KCABCH7B
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
7KCAB

Registered Owner (Current)

Name
WALLACE AVIATION INC
Address
PO BOX 126
City
WALLACE
State / Zip Code
NE 69169-0126
Country
United States

Analysis

On February 23, 2010, approximately 1500 mountain standard time, a Champion 7KCAB, N5065X,registered to and operated by the private pilot, was substantially damaged when the fabric on the upper right wing tore off while the airplane was being maneuvered near Greeley, Colorado. Visual meteorological conditions prevailed at the time of the accident. The personal flight was being conducted under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91 without a flight plan. The pilot, the sole occupant, was not injured. The local flight originated at Greeley approximately 1430.

According to the pilot’s accident report, he was practicing steep turns around a point at 7,500 feet msl. During one of the turns, he heard an unusual sound and saw something falling away from the aircraft. He then noticed a piece of fabric “flapping” in the slipstream at the trailing edge of the right aileron. The airplane developed a slight sink rate, but the engine and flight controls operated normally. He returned to Greeley and made an uneventful landing.

Post-flight inspection disclosed that nearly 80 percent of the fabric on the top of the right wing had separated, and several ribs were damaged when the rivets separated with the fabric. Several other ribs were distorted from slipstream.

The airplane had been used for fish spotting in Alaska. According to the maintenance records, the airframe was last recovered on July 21, 2003 at a total time of 3,894.0 hours. Fabric punch tests since that recovering had been satisfactory.

The Denver NTSB was notified of this accident on April 10, 2010. The pilot offered no explanation as to why he didn't report the accident promptly in accordance with Title 49 CFR 830.5(a).

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN10LA198