N6630X

Substantial
Minor

CESSNA 210AS/N: 21057630

Accident Details

Date
Friday, May 21, 2010
NTSB Number
WPR10LA251
Location
Benson, AZ
Event ID
20100522X11639
Coordinates
31.999444, -110.357780
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

A loss of engine power due to fuel starvation as a result of a loss of fuel pressure caused by the fuel pump screws being loose. Contributing to the accident was inadequate maintenance.

Aircraft Information

Registration
N6630X
Make
CESSNA
Serial Number
21057630
Engine Type
Reciprocating
Year Built
1960
Model / ICAO
210AC210
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
TRI ROTOR AG SERVICES
Address
PO BOX 498
Status
Deregistered
City
SOMERTON
State / Zip Code
AZ 85350-0498
Country
United States

Analysis

On May 21, 2010, about 1030 mountain standard time, a Cessna 210A, N6630X, lost engine power during approach to landing at Benson Municipal Airport (E95), Benson, Arizona. The airplane subsequently collided with terrain during the off airport landing, substantially damaging the left wing. The pilot was operating the airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The private pilot and one passenger received minor injuries. The local personal flight departed Benson about 1130. Visual meteorological conditions prevailed, and no flight plan had been filed.

The pilot reported that he extended the downwind leg of the traffic pattern to test the landing gear warning system before he turned to the base leg. As the pilot initiated a turn to final, the engine suddenly lost power. The pilot scanned all of the gauges and confirmed the fuel selector valve was on the fullest fuel tank; he then turned on the boost pump and attempted to restart the engine, but was unsuccessful. The pilot observed a nearby road and attempted to land on it, however, the airplane landed short onto a ridge. Both the left main landing gear and the nose wheel landing gear were sheared off and the airplane slid on its nose until it came to a rest.

Post accident examination of the engine by a certificated airframe and powerplant mechanic and a Federal Aviation Administration inspector reported that the fuel system was tested and the diaphragm in the fuel manifold valve was found to be brittle and stiff. The engine driven fuel pump had fuel stains on it, and when further inspected, the four screws that hold the body of the fuel pump together were found loose. The pump was submerged in fuel and manually rotated with a drill motor at 2,000 rpm; it emitted fuel along with large air bubbles. The four screws were tightened and the pump was again submerged in the fuel; it flowed normally without any air bubbles present.

Examination of the airplane records indicated that an annual inspection had been completed on February 1, 2010, with a reported tach time of 4,736.7. The tach time at the time of the accident was 4,747.8.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR10LA251