N9049SGINGERICH ALTON & SLAGEL DEAN CHRISTAVIA MK 12010-10-01 NTSB Accident Report

Substantial
None

GINGERICH ALTON & SLAGEL DEAN CHRISTAVIA MK 1S/N: 1001

Summary

On October 01, 2010, a Gingerich Alton & Slagel Dean CHRISTAVIA MK 1 (N9049S) was involved in an incident near Nappanee, IN. All 1 person aboard were uninjured. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this incident to be: The total loss of engine power for undetermined reasons.

The pilot reported that after takeoff, about 250 feet above ground level (agl), the engine "suddenly cut out." He reduced the throttle to idle and attempted to land on the runway; however, there was not enough distance remaining. He subsequently pushed the throttle forward and the engine regained power. As the airplane reached approximately 250 feet agl, the engine lost power again. The pilot subsequently set up for a forced landing to a harvested corn field immediately west of the airport. The airplane nosed over during the emergency landing. A post accident examination of the engine did not reveal any anomalies consistent with a pre-impact failure or malfunction.

This incident is documented in NTSB report CEN11CA002. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N9049S.

Accident Details

Date
Friday, October 1, 2010
NTSB Number
CEN11CA002
Location
Nappanee, IN
Event ID
20101004X45616
Coordinates
41.446109, -85.934722
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The total loss of engine power for undetermined reasons.

Aircraft Information

Registration
Make
GINGERICH ALTON & SLAGEL DEAN
Serial Number
1001
Engine Type
Reciprocating
Model / ICAO
CHRISTAVIA MK 1DH8A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
CHRISTAVIA MK 1

Registered Owner (Current)

Name
KNOX PHILLIP ALLEN II
Address
26435 MADISON RD
City
NORTH LIBERTY
State / Zip Code
IN 46554-9426
Country
United States

Analysis

The pilot reported that after takeoff, about 250 feet above ground level (agl), the engine "suddenly cut out." He reduced the throttle to idle and attempted to land on the runway; however, there was not enough distance remaining. He subsequently pushed the throttle forward and the engine regained power. As the airplane reached approximately 250 feet agl, the engine lost power again. The pilot subsequently set up for a forced landing to a harvested corn field immediately west of the airport. The airplane nosed over during the emergency landing. A post accident examination of the engine did not reveal any anomalies consistent with a pre-impact failure or malfunction. The pilot noted that his intention was to stay in the airport traffic pattern in order to practice takeoffs and landings because it had been approximately 6 months since he had flown the airplane.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN11CA002