N6781X

Substantial
None

CESSNA 310FS/N: 310-0081

Accident Details

Date
Friday, April 1, 2011
NTSB Number
ERA11LA221
Location
Sanford, FL
Event ID
20110403X60004
Coordinates
28.780307, -81.270492
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The failure of the nose landing gear due to inadequate servicing of the nose gear strut reservoir.

Aircraft Information

Registration
N6781X
Make
CESSNA
Serial Number
310-0081
Engine Type
Reciprocating
Year Built
1961
Model / ICAO
310FC310
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
SON & MOON INC
Address
213 BURGESS DR
Status
Deregistered
City
WINTER SPRINGS
State / Zip Code
FL 32708-5190
Country
United States

Analysis

On April 1, 2011, at 1545 eastern daylight time, a Cessna 310F, N6781X, registered to a private individual, incurred substantial damage to the fuselage after the nose gear collapsed during landing rollout at Sanford Orlando International Airport (SFB), Sanford, Florida. The certified flight instructor (CFI) and his private pilot-rated dual student were not injured. The instructional flight was conducted under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed. The flight originated from SFB at 1500.

The CFI reported that after takeoff, while retracting the landing gear, a loud “bang” was heard. It was assumed by the CFI that the noise came from the landing gear doors closing into each other. The gear-up light illuminated indicating that the landing gear were retracted and the doors were closed. The flight returned to SFB for two planned landings; first a touch-and-go and then a full stop. On the first landing; the gear were extended and a gear-down light illuminated. A touch-and-go was conducted without incident. Upon extending the gear for the second landing, the gear-down light failed to illuminate. The landing gear were recycled, and the gear light gave a gear-up indication. Another gear extension was attempted, and a gear-down indication was not received. The CFI contacted the SFB tower to request a low fly-by for a visual inspection of the gear position. The tower controller reported all three gear were down and the airplane was cleared to land. The touchdown on the main gear was normal; but as weight was applied to the nose wheel, the nose gear collapsed.

The airplane was examined by a Federal Aviation Administration (FAA) inspector under the direction of a NTSB investigator. The airplane was raised using aircraft jacks to take the weight off of the wheels. The nose gear shock strut trunnion assembly remained in the compressed position. Approximately one inch of the strut trunnion surface was visible. An attempt to retract the nose landing gear was unsuccessful, due to the strut fork assembly coming into contact with the nose landing gear door attachment brackets. The nose strut trunnion was manually extended out of the cylinder until approximately three inches of the piston surface was visible. The nose landing gear assembly was then manually raised up into the wheel well area and fully retracted. The nose landing gear strut trunnion reservoir was checked for air pressure and was totally empty of air. The strut trunnion reservoir was checked for fluid which was found to be very low. There were no signs of fluid leakage around the nose landing gear strut trunnion. A review of the maintenance logbooks did not reveal any prior discrepancies with the nose landing gear assembly.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA11LA221