N7849Y

Substantial
None

PIPER PA-30S/N: 30-929

Accident Details

Date
Sunday, April 3, 2011
NTSB Number
CEN11LA262
Location
Ruidoso, NM
Event ID
20110403X64126
Coordinates
33.460834, -105.529998
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The left engine's intermittent loss of power during initial climb for undetermined reasons. Contributing to the accident was the high density altitude at the time of the accident.

Aircraft Information

Registration
N7849Y
Make
PIPER
Serial Number
30-929
Engine Type
Reciprocating
Year Built
1965
Model / ICAO
PA-30PA30
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
SALE REPORTED
Address
635 AIRPORT RD
Status
Deregistered
City
GREELEY
State / Zip Code
CO 80631-9148
Country
United States

Analysis

On April 3, 2011, about 1300 mountain daylight time, a Piper PA-30, N7849Y, experienced an intermittent loss of left engine power during initial climb from the Sierra Blanca Regional Airport (SRR), Ruidoso, New Mexico. The airline transport pilot subsequently executed a forced landing and neither he nor the passenger was injured. The airplane sustained substantial damage to the fuselage and both wings. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed and a flight plan had not been filed for the cross-country flight destined for the Eagle's Nest Estates Airport (2TS6), Midlothian, Texas.

According to the pilot, around 200-feet above ground level (AGL), the airplane's left engine began operating intermittently with reduced power. The pilot added that because of the partial loss of engine power, along with high density altitude, turbulence, and wind shear, he was unable to maintain altitude. The airplane collided with the airport's perimeter fence and the left wing struck a tree. Subsequently, the airplane impacted the ground and came to rest in an upright position in a field adjacent to the airport.

Logbook entries provided to the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), documented previous occurrences where the left engine experienced partial power loss. An entry dated December 11, 2009, reported that the left engine would not reach expected static RPM and that it ran "rough." The fuel flow divider was removed, cleaned, and reinstalled. The engine would then reach expected static RPM and was returned to service. An entry on February 2, 2010, stated that the airplane was landed due to a "rough' running left engine. Following the discovery of fuel contamination, the fuel system was flushed and the engine returned to service.

An airframe and powerplant mechanic (A&P), with an inspection authorization (IA), examined both engines. Engine continuity was established through each engine and the magnetos produced spark when rotated. A differential cylinder compression test was performed on each cylinder. The right engine cylinders ranged from 65 to 72 PSI over 80 PSI and the left engine cylinders ranged from 62 to 68 PSI over 80 PSI. Both inlet air filters, along with the fuel servo inlet screens, were found to be unobstructed. The mechanic reported that no abnormalities were noted that would have prevented either engine from producing power.

The airplane's weight at the time of the accident was calculated to be approximately 231 pounds below the maximum gross weight of 3,600 pounds. In addition, the center of gravity (CG) was calculated to be within limits. Per the pilot operating handbook (POH), the service ceiling for the airplane was listed as 18,600 feet density altitude and the single-engine service ceiling as 5,800 feet density altitude. The calculated density altitude around the time of the accident was 9,040 feet.

At 1315, the automated weather observing system at SRR reported, wind from 230 degrees at 37 knots with gust to 46 knots, 10 miles visibility, clear of clouds, temperature 68 degrees Fahrenheit, dew point 16 degrees Fahrenheit, and a barometric pressure setting of 29.86 inches of Mercury.

The reason for the left engine's intermittent loss of power could not be determined.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN11LA262