Summary
On May 11, 2011, a Beech B24R (N9321S) was involved in an incident near Dowagiac, MI. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The flight instructor's failure to maintain an appropriate glide path and airspeed during the landing approach, which resulted in an aerodynamic stall.
The certified flight instructor (CFI) was demonstrating a power off spot landing to the dual student. The student held a commercial pilot certificate and was observing the maneuver at the time of the accident. The CFI stated that he made one attempted power off spot landing that ended in a go-around because the airplane would not have made it to the runway. He stated that on the second attempt, he again would not make it to the 1,000 foot runway markings he was aiming for, but felt that he would make it to the runway. The CFI stated that he started to add engine power when the airplane was about 30 feet from the runway end and 10 feet above the ground, but it "dropped into the sod." The airplane's left landing gear separated from the wing, and the left wing separated from the fuselage.
This incident is documented in NTSB report CEN11CA362. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N9321S.
Accident Details
Probable Cause and Findings
The flight instructor's failure to maintain an appropriate glide path and airspeed during the landing approach, which resulted in an aerodynamic stall.
Aircraft Information
Registered Owner (Historical)
Analysis
The certified flight instructor (CFI) was demonstrating a power off spot landing to the dual student. The student held a commercial pilot certificate and was observing the maneuver at the time of the accident. The CFI stated that he made one attempted power off spot landing that ended in a go-around because the airplane would not have made it to the runway. He stated that on the second attempt, he again would not make it to the 1,000 foot runway markings he was aiming for, but felt that he would make it to the runway. The CFI stated that he started to add engine power when the airplane was about 30 feet from the runway end and 10 feet above the ground, but it "dropped into the sod." The airplane's left landing gear separated from the wing, and the left wing separated from the fuselage. The CFI reported no mechanical failures or malfunctions.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN11CA362