C-GLHQ

Substantial
None

HUGHES 500DS/N: 200662D

Accident Details

Date
Monday, June 27, 2011
NTSB Number
ANC11CA056
Location
Ambler, AK
Event ID
20110630X35227
Coordinates
67.099998, -157.850006
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's misalignment of the helicopter on the landing structure.

Aircraft Information

Registration
Make
HUGHES
Serial Number
200662D
Engine Type
Turbo-shaft
Year Built
1980
Model / ICAO
500DH500
Aircraft Type
Rotorcraft
No. of Engines
1
FAA Model
369D

Registered Owner (Current)

Name
9348-8260 Québec inc.
Address
804, avenue du Lac
City
Preissac
State / Zip Code
Quebec J0Y2E-0
Country
United States

Analysis

The helicopter pilot landed a high skid, turbine-powered helicopter at a remote drilling site, and the three passengers disembarked. The remote landing site was constructed of 6-inch by 6-inch wooden beams, which required that the pilot land perpendicular to and on the beams with the helicopter's skids. The pilot reported that after landing he retarded the engine throttle to flight idle to begin the mandatory 2 minute engine cool down procedure. He then got out of the helicopter to check the placement of the helicopter's skids on the beams, and it subsequently tipped backwards, with the tail rotor striking terrain. In his written statement to the NTSB, the pilot wrote, in part: "While waiting, I stepped out of the helicopter to look under the helicopter to verify that my bear paws were both securely placed on the supporting timber. Within a moment of stepping out, I noticed movement and watched as the helicopter tipped backwards until it came to rest on the tail rotor and stinger." A postaccident inspection revealed that while landing, the pilot inadvertently placed the helicopter's skids behind the aft wooden beam, and the helicopter tipped backwards once the pilot exited the helicopter. The pilot said there were no preimpact mechanical problems with the helicopter. The helicopter sustained substantial damage to the tail boom, tail rotor drive system, and tail rotor gearbox.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC11CA056