N866P

Substantial
None

BEECH 35-C33S/N: CD-1023

Accident Details

Date
Wednesday, March 21, 2012
NTSB Number
WPR12LA147
Location
St. George, UT
Event ID
20120327X44242
Coordinates
37.102795, -113.562530
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The total loss of engine power due to the loose mixture control arm.

Aircraft Information

Registration
Make
BEECH
Serial Number
CD-1023
Engine Type
Reciprocating
Year Built
1966
Model / ICAO
35-C33BE33
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
35-C33

Registered Owner (Current)

Name
NOSLER CAMERON
Address
10905 WINTER TEAL AVE
City
LAS VEGAS
State / Zip Code
NV 89144-1458
Country
United States

Analysis

On March 21, 2012, about 0930 mountain daylight time, a Beech 35-C33, N866P, sustained substantial damage during a forced landing near St. George, Utah. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91. The commercial pilot and his passenger were not injured. Visual meteorological conditions prevailed and no flight plan was filed for the personal cross-country flight which originated from St. George about 0905 with an intended destination of Phoenix, Arizona.

In a written statement to the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), the pilot reported that while in cruise flight at about 9,500 feet mean sea level (about 4,500 feet above ground level), the engine’s exhaust gas temperature was hotter than normal, and the fuel flow was lower than normal. Suddenly, all engine power was lost. The pilot stated that he attempted to restart the engine, but he was not successful. During the subsequent forced landing, the pilot landed the airplane gear up on a road.

Postaccident examination of the airplane revealed that the firewall and a bulkhead were bent. The airplane was recovered to a secure location for further examination.

Examination of the engine by a representative from Continental Motors Inc. and a Federal Aviation Administration (FAA) inspector under the supervision of the NTSB IIC revealed that the fuel metering unit was undamaged. The throttle control arm moved freely by hand. The mixture control arm moved freely by hand with no associated movement of the fuel control shaft and nut. The mixture control cable was removed and the mixture control arm was found loose on the control shaft. A recordable digital torque wrench was used to record the back-off torque from the nut. The recordable torque wrench records from 24 to 240 inch/lbs. There was no indication of torque found on the nut. The mixture control arm was removed from the shaft. The control arm machined chamfer had formed splines and exhibited deformation and movement of material. The nut and control arm mating surfaces showed rub marks. No evidence of any additional mechanical malfunctions was found during the engine examination.

Review of the airplane logbook maintenance records revealed that the airframe and engine underwent the most recent annual/100-hour inspection on October 19, 2011, at an airframe total time of 5,840 hours and engine time since major overhaul of 1,165 hours. The pilot reported he had flown the airplane about 22 hours since the annual inspection.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR12LA147