N7171P

Substantial
None

PIPER PA-24-250S/N: 24-2339

Accident Details

Date
Monday, May 14, 2012
NTSB Number
CEN12LA299
Location
Shawnee, OK
Event ID
20120514X33812
Coordinates
35.357223, -96.943336
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The improper installation of the mixture cable by maintenance personnel, which allowed the mixture cable to entangle with the landing gear during gear extension and led to the subsequent loss of engine power.

Aircraft Information

Registration
N7171P
Make
PIPER
Serial Number
24-2339
Engine Type
Reciprocating
Year Built
1961
Model / ICAO
PA-24-250PA24
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BOTT DAVID F
Address
PO BOX 721145
Status
Deregistered
City
OKLAHOMA CITY
State / Zip Code
OK 73172-1145
Country
United States

Analysis

On May 14, 2012, approximately 1330 central daylight time, a Piper PA-24-250 airplane, N7171P, was substantially damaged during a forced landing to a field near Shawnee, Oklahoma. The private pilot was not injured. The airplane was registered to and operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a ferry flight. Visual meteorological conditions prevailed for the flight, which operated without a flight plan. The flight originated from Sundance Airpark (KHSD), Oklahoma City, Oklahoma, approximately 1315, and was en route to Shawnee Regional Airport (KSNL), Shawnee, Oklahoma.

On final approach, the pilot lowered the landing gear handle; however, he did not receive confirmation that the landing gear was down and locked. The pilot stated that "a lot of force" was required to conduct the manual gear override, but he was not able to get the handle up. Shortly thereafter, the engine lost power. The pilot performed a gear up, forced landing to a field. During the landing, the right wing was buckled and the firewall was wrinkled.

According to the Federal Aviation Administration inspector who traveled to the scene, the mixture cable was bent and would not move. The routing of the mixture cable did not match assembly drawings. The mixture cable was found separated from its last clamp prior to the carburetor mixture control and the mixture control was found in the cutoff position. He also noted that several clamps normally used to route the mixture cable were not present. A grease fitting on the over center link for the nose landing gear was in line with the bend in the mixture cable.

According to the pilot, the engine had just been removed and reinstalled for an engine overhaul.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN12LA299