N1875N

Substantial
None

CESSNA 120S/N: 12119

Accident Details

Date
Friday, June 8, 2012
NTSB Number
WPR12LA262
Location
Smith Valley, NV
Event ID
20120614X21912
Coordinates
38.833332, -119.395553
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The failure of the right main landing gear strut due to corrosion-induced fatigue, which resulted in a runway excursion.

Aircraft Information

Registration
N1875N
Make
CESSNA
Serial Number
12119
Engine Type
Reciprocating
Year Built
1946
Model / ICAO
120C120
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
3011 W BUCKEYE RD
Status
Deregistered
City
PHOENIX
State / Zip Code
AZ 85009-5734
Country
United States

Analysis

On June 8, 2012, about 1015 Pacific daylight time, a Cessna 120, N1875N, experienced a runway excursion during landing at Farias Wheel Airport (NV33), Smith Valley, Nevada. Valley View Flyers LLC was operating the airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The private pilot was not injured; the airplane sustained substantial damage. The cross-country personal flight departed Yerington, Nevada, about 0955, with a planned destination of NV33. Visual meteorological conditions prevailed, and no flight plan had been filed.

The pilot reported that during landing the airplane bounced; when it touched down again, it suddenly veered to the left. He applied power to abort the landing, but the airplane continued left, and departed the runway surface into sagebrush. The right main landing gear collapsed, and the right wing and the propeller contacted the ground. The pilot turned off the master switch, shut off the fuel, and exited the airplane.

A Federal Aviation Administration (FAA) inspector examined the wreckage on site. He noted that the fracture surface of the right main landing gear was flat with beach marks. The part was submitted to the National Transportation Safety Board (NTSB) Materials Laboratory for examination.

An NTSB metallurgist observed that the main landing gear strut was transversely fractured through the upper attachment hole for the step bracket. The upper fracture face was mechanically damaged, while the lower face was mostly undamaged. Optical examinations of the fractured face revealed chevron markings indicative of fracture initiation on both sides of the hole at the corners formed by the hole’s bore and the upper surface of the strut. Closer magnified examinations uncovered small fatigue cracks at both corners of the hole. The fatigue on the forward side of the hole initiated at three locations in a corrosion pitted area of the bore surface. The aft fatigue region initiated at a single origin at the corner in a corroded area. Corrosion was visible in unpainted areas. Removing the remnant paint from the bore revealed corrosion and corrosion pitting over the entire bore surface.

The airplane was built in 1946, and had a total airframe time of 8,934 hours.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR12LA262