N619BA

MINR
None

FAIRCHILD SA227-ACS/N: AC619B

Accident Details

Date
Saturday, November 10, 2012
NTSB Number
CEN13IA059
Location
Minneapolis, MN
Event ID
20121118X34829
Coordinates
44.875831, -93.219718
Aircraft Damage
MINR
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Loose electrical connections to the hydraulic system and anomalies in the hydraulic shuttle valve and power pack, which resulted in an uncommanded gear unlock and collapse of the left main landing gear. Contributing to the accident was the operator’s failure to comply with the life limits outlined by the hydraulic power pack’s manufacturer.

Aircraft Information

Registration
Make
FAIRCHILD
Serial Number
AC619B
Engine Type
Turbo-prop
Year Built
1985
Model / ICAO
SA227-AC
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
12
FAA Model
SA227-AC

Registered Owner (Current)

Name
BEMIDJI AVIATION SERVICES INC
Address
4125 HANGAR DR NW
City
BEMIDJI
State / Zip Code
MN 56601-6243
Country
United States

Analysis

On November 9, 2012, about 2007 central standard time, N619BA, a Fairchild Aircraft, Inc., SA227-AC, multi-engine airplane, sustained minor damage when the left main landing gear collapsed during landing at Minneapolis St. Paul International Airport (MSP), Minneapolis, Minnesota. The pilot was not injured. The airplane was registered to and operated by Bemidji Aviation Services, Inc. Night visual meteorological conditions (VMC) prevailed at the time of the accident and an instrument flight rules (IFR) flight plan had been filed for the 14 Code of Federal Regulations Part 135 scheduled cargo flight. The airplane departed Duluth International Airport (DLH), Duluth, Minnesota, about 1926 destined for MSP.The pilot reported that all three green landing gear indicator lights were illuminated before he performed an otherwise normal landing. About 50 to 100 feet after touching down on the runway, the left main landing gear collapsed. The airplane skidded off of the left side of runway and came to rest upright in the grass. A postincident examination of the airplane found two loose electrical connections to the hydraulic system. An overhaul teardown of the hydraulic shuttle valve showed the seat out of tolerance, cap safety wire holes damaged and a washer not to the current revisions. The washer also showed corrosion. An examination of the hydraulic power pack revealed a washer not to the current revision. The system operated normally after the electrical wiring was repaired, and the hydraulic power pack and shuttle valve were replaced.

The operator reported that they have revised their life limitations on the hydraulic power pack so that it now complies with the instructions in the manufacturer's service letter.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN13IA059