N169LJ

Substantial
Minor

CESSNA 208BS/N: 208B0599

Accident Details

Date
Monday, December 3, 2012
NTSB Number
ANC13LA012
Location
Mekoryuk, AK
Event ID
20121204X63622
Coordinates
60.400001, -166.336944
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
8
Total Aboard
9

Probable Cause and Findings

The total loss of engine power as a result of a fractured first-stage compressor blade due to fatigue cracking. The source of the fatigue crack could not be determined due to secondary damage sustained to the fracture surface.

Aircraft Information

Registration
N169LJ
Make
CESSNA
Serial Number
208B0599
Engine Type
Turbo-shaft
Year Built
1997
Model / ICAO
208BC208
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
PROPS & JETS INC
Address
3500 S DUPONT HWY
Status
Deregistered
City
DOVER
State / Zip Code
DE 19901-6041
Country
United States

Analysis

On December 3, 2012, about 1050 Alaska standard time, a Cessna 208B airplane, N169LJ, sustained substantial damage during a forced landing shortly after takeoff from the Mekoryuk Airport, Mekoryuk, Alaska. Of the nine people aboard, the two pilots and six passengers were not injured, and one passenger sustained minor injuries. The airplane was being operated as Flight 140, by Hageland Aviation Services, Inc., dba ERA Alaska, Anchorage, Alaska, as a visual flight rules (VFR) scheduled commuter flight under the provisions of 14 Code of Federal Regulations (CFR) Part 135. Visual meteorological conditions prevailed, and company flight following procedures were in effect. The flight originated at the Mekoryuk Airport about 1045, and was destined for Bethel, Alaska.In a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC), the pilot-in-command (PIC) stated that the second-in-command (SIC) was the flying pilot for the flight to Bethel. He said that the takeoff and initial climb were normal, but shortly after passing 1,000 feet, the engine "coughed," started vibrating, and lost power. An attempt to restart the engine was not successful. The PIC assumed control of the airplane, and landed on a frozen bay approximately 5 miles northeast of the Mekoryuk Airport. Witnesses at the airport observed the airplane descending, and responded with snow machines, and all-terrain vehicles to transport the airplane's occupants back to Mekoryuk.

During the forced landing the airplane sustained substantial damage to the fuselage and right wing.

The airplane was equipped with a Pratt & Whitney PT6A-114A turbine engine. A postaccident engine examination, performed at the facilities of Pratt & Whitney Canada, St. Hubert, Quebec, Canada, and under the direction of a senior NTSB powerplants investigator, revealed that a blade on the first stage compressor rotor failed as a result of a fatigue fracture. The fatigue crack initiated from the leading edge area and then propagated towards the trailing edge, and at mid-chord, the blade released by tensile overload. The initiation of the fracture could not be determined because of secondary damage to the fracture surface. A copy of the Safety Board powerplants investigator's report is included in the public docket for this incident.

During the last engine overhaul, 5 first stage compressor blades were replaced with new blades. The blade that failed during the accident flight was one of the five replaced blades based on the batch numbers recorded on the blades.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC13LA012