Accident Details
Probable Cause and Findings
The flight crew's failure to maintain terrain clearance, which resulted in controlled flight into terrain in instrument meteorological conditions. Contributing to the accident were the flight crew's failure to correctly read back and interpret clearance altitudes issued by the air traffic controller, their failure to adhere to minimum altitudes depicted on the published instrument approach chart, and their failure to adhere to company checklists. Also contributing to the accident were the air traffic controller's issuance of an ambiguous clearance to the flight crew, which resulted in the airplane's premature descent, his failure to address the pilot's incorrect read back of the assigned clearance altitudes, and his failure to monitor the flight and address the altitude violations and issue terrain-based safety alerts.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHT
On March 8, 2013, about 0815 Alaska standard time, a Beech 1900C airplane, N116AX, operating as Alaska Central Express flight 51, was destroyed when it collided with rising terrain about 10 miles east of Aleknagik, Alaska. The captain and first officer were fatally injured. Flight 51 was a cargo flight operating under the provisions of 14 Code of Federal Regulations (CFR) Part 135. Instrument meteorological conditions (IMC) prevailed along the route of flight, and the airplane was operating on an instrument flight rules (IFR) flight plan. The flight departed King Salmon Airport, King Salmon, Alaska, about 0750, and was en route to Dillingham Airport (DLG), Dillingham, Alaska.
A postaccident review of Federal Aviation Administration (FAA) radar data and radio communication recordings revealed that, about 0803, the pilot requested the RNAV/GPS runway 19 approach to DLG and asked for routing directly to ZEDAG, the initial approach fix (IAF). At the time of the pilot's request, the airplane was about 30 miles southeast of ZEDAG at an altitude of about 5,900 feet mean sea level (msl). The on-duty Anchorage Air Route Traffic Control Center (ARTCC) radar controller cleared the airplane to fly directly to ZEDAG followed by the ZEDAG transition and the RNAV/GPS runway 19 approach. The controller told the pilot to maintain an altitude "at or above 2,000 feet msl until established on a published segment of the approach." The pilot read back, "Maintain two thousand until a published segment of the approach." About 6 minutes later, as the airplane descended toward the IAF, the pilot requested to enter the holding pattern while checking on runway conditions on another radio frequency, and the controller granted the request. At the time of the pilot's request, the airplane was at an altitude of about 2,200 feet msl. The airplane subsequently disappeared from the controller's radar display, and all contact with the flight was lost.
At 0830, the on-duty ARTCC operations manager notified the Anchorage rescue coordination center (RCC) of the missing airplane, and, at 0835, the FAA issued an alert notice. About 0854, a 406-MHz beacon activation notification was received by the RCC, and search and rescue operations were initiated. Initial attempts to reach the accident site were hampered by poor weather conditions.
On March 9, about 0606, aerial searchers located the accident site about 6 miles north-northwest of ZEDAG in an area of steep, snow and ice-covered terrain known as "the Muklung Hills." About 0703, a ground search party reached the accident site, which was at an elevation of about 1,996 feet msl.
FLIGHT CREW INFORMATION
Captain
The captain, age 38, held an airline transport pilot certificate with an airplane multiengine land rating and commercial pilot privileges with an airplane single-engine land rating and a type rating in the Beech 1900. His most recent first-class FAA medical certificate was issued June 11, 2012, with no limitations.
The captain was hired by Alaska Central Express on July 18, 2008, and, at that time, he had 260 hours of total flight experience. He completed his initial company training, including Beech 1900 second-in-command (SIC) ground training, on July 28, 2008, and was assigned to fly as SIC of Beech 1900 airplanes at the company's base in Anchorage. On September 7, 2011, he was upgraded to a Beech 1900 captain. The operator reported that the captain had accumulated 5,770 total flight hours, including 5,470 hours in the accident airplane make and model. His most recent airman competency/proficiency check, which was administered by a company check airman, was completed on October 20, 2012.
On March 5, the captain's duty day started at 0330 and ended at 1130, and he flew 4.4 hours. On March 6, his duty day started at 0330 and ended at 1300, and he flew 4.5 hours. On March 7, his duty day started at 0430 and ended at 1000, and he flew 3.3 hours. On March 8, the day of the accident, his duty day started at 0430, and he flew 1.6 hours before the accident.
First Officer
The first officer, age 21, held a commercial pilot certificate with airplane single-engine land, multiengine land, and instrument airplane ratings. His most recent FAA second-class medical certificate was issued August 9, 2012, with no limitations.
The first officer was hired by Alaska Central Express on November 12, 2012, and, at that time, he had 220 hours of total flight experience. He completed his initial company training, including Beech 1900 SIC ground and flight training, on November 30, 2012, and was assigned to fly as SIC of Beech 1900 airplanes at the company's base in Anchorage. The operator reported that the first officer had accumulated 470 total flight hours, including 250 hours in the accident airplane make and model. His most recent airman competency/proficiency check, which was administered by a company check airman, was completed on December 1, 2012.
On March 5, the first officer's duty day started at 1100 and ended at 2200, and he flew 7.4 hours. On March 6, his duty day started at 1200 and ended at 1930, and he flew 4.2 hours. On March 7, he was off duty. On March 8, the day of the accident, his duty day started at 0430, and he flew 1.6 hours before the accident.
AIRCRAFT INFORMATION
The airplane, manufactured in 1992, was a twin-engine Beech 1900C equipped with retractable landing gear, two Pratt and Whitney PT6A-65B engines, and controllable-pitch propellers. Alaska Central Express maintained the airplane in accordance with an approved continuing airworthiness program, and the most recent required inspection was completed on March 7, 2013, when the airplane had accumulated 29,824 total hours.
The airplane was equipped with a Bendix/King KMD 850 multifunction display capable of providing audible and visual terrain warnings. The airplane was also equipped with dual Garmin 430W units capable of providing visual terrain warnings. Both warnings could be inhibited by the flight crew.
The airplane was equipped for instrument flight into icing conditions and could be operated by a single pilot. The airplane was not equipped with, nor was it required to be equipped with, a cockpit voice recorder or a flight data recorder.
WRECKAGE AND IMPACT INFORMATION
The airplane's wreckage was located in an area of steep, ice and snow-covered terrain on a southeast-facing slope. The terrain was rough and uneven, and high-wind conditions after the accident had created areas of drifted snow, moved lighter pieces of debris, and buried some debris. The initial impact point was at an elevation of about 1,996 feet, and the debris path extended about 900 feet uphill to an elevation of about 2,300 feet in a triangular/fan shape. About 700 feet from the initial point of impact, the major debris field was more than 400 feet wide, and single pieces of debris could be seen at greater distances in all directions. The debris path was on a magnetic heading of about 340 degrees. According to topographic maps, the peak elevation is 2,550 feet. The initial impact point was a rock outcrop protruding from the snow. Metal scrapings were found on the rock surface consistent with damage observed on the center of the airplane's fuselage. No indications of any wing impact were found near the initial impact point. The first structural piece was located about 400 feet from the initial impact point. Large sections of fuselage and expelled cargo were located about 525 feet from the initial impact point. The fuselage and cockpit were found separated into three large pieces.
Subsequent examination of the engines and propellers indicated that the propeller blades had all sheared off at the propeller hub, and the engines' exhausts exhibited signs of hot metal folding.
Damage to the Bendix/King KMD 850 and dual Garmin 430W units precluded testing, and the preaccident configuration of the units (including which functions were enabled or inhibited by the flight crew) could not be determined.
MEDICAL AND PATHOLOGICAL INFORMATION
Captain
A postmortem examination of the captain was performed under the authority of the Alaska State Medical Examiner in Anchorage on March 11, 2013. The cause of death was reported as multiple blunt force injuries sustained in an airplane crash, and the manner of death was an accident. However, the autopsy identified severe coronary artery disease with greater than 85% stenotic lesion in the distal left anterior descending artery. Nevertheless, there was no suggestion of medical impairment or incapacitation related to the probable cause of the accident.
A toxicological examination by the FAA's Civil Aeromedical Institute (CAMI), Oklahoma City, Oklahoma, on April 30, 2013, revealed dextrorphan and doxylamine in urine and 0.016 ug/ml doxylamine in blood.
According to CAMI doxylamine is a sedating antihistamine available over the counter and by prescriptions and used to treat cold and allergy symptoms. Its therapeutic window is 0.050 to 0.150 ug/ml and it carries the following warning: "May impair mental and/or physical ability required for the performance of potentially hazardous tasks (e.g., driving, operating heavy machinery)." The absence of dextromethorphan or its metabolite in the blood suggests the cough suppressant was no longer having any effect on the captain.
Given that the toxicology testing identified a level well below the therapeutic window, there is no evidence that it was impairing the captain at the time of the accident.
First Officer
A postmortem examination of the first officer was performed under the authority of the Alaska State Medical Examiner in Anchorage on March 11, 2013. The cause of death was reported as multiple blunt force injuries sustained in an airplane crash. The manner of death was an accident.
A toxicological examination by CAMI on April 18, 2013, was negative for any alcohol or drugs.
METEOROLOGICAL INFORMATION
The DLG weather observation at ...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ANC13FA030