N92319

Substantial
None

FRANKE RUSSELL J SEAREYS/N: 1DK109

Accident Details

Date
Thursday, April 11, 2013
NTSB Number
ERA13LA198
Location
Polk City, FL
Event ID
20130412X91833
Coordinates
28.168888, -81.817779
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

An inadvertent encounter with the water wake from a larger amphibious airplane before takeoff and the pilot's subsequent inadequate preflight inspection of the airplane during which he failed to note damage caused by the wake encounter.

Aircraft Information

Registration
Make
FRANKE RUSSELL J
Serial Number
1DK109
Engine Type
Reciprocating
Year Built
1996
Model / ICAO
SEAREYBPAT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
SEAREY

Registered Owner (Current)

Name
BERRY JIMMY O
Address
PO BOX 951
City
LEXINGTON
State / Zip Code
SC 29071-0951
Country
United States

Analysis

On April 11, 2013, about 1500 eastern daylight time, an experimental amateur-built Searey, N92319, incurred substantial damage during a water taxi, and control binding and additional substantial damage after the subsequent takeoff from Lake Agnes, Polk City, Florida. The private pilot and the passenger were not injured. Visual meteorological conditions prevailed. No flight plan had been filed for the flight, between Lake Agnes and Florida Flying Gators Ultralight Flightpark (3FD4), Groveland, Florida. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91.According to the pilot, he taxied the airplane down a boat ramp, following a 1950's Piaggio twin-engine amphibian that weighed in excess of 6,000 pounds. The Piaggio took off, and the Searey then encountered a 2- to 3-foot wake. The pilot "quartered" the Searey into the wake, and when he did, the right side pitched up, and the left side pitched down.

The pilot subsequently looked at the left horizontal stabilizer via a mirror on the airplane's left wing strut and conducted a full flight control check with no anomalies noted. He then took off, with the airplane bouncing once along the choppy water surface before becoming airborne.

Once airborne, the pilot noted pitch control problems and was not able to level off the airplane until it reached about 1,800 feet. He was then able to descend the airplane at a rate of about 50 feet per minute by maintaining airspeed just above stall.

The pilot circled the lake six times before being able to land. The landing included two bounces of the right wing, and during the second bounce, the right horizontal stabilizer was substantially damaged when it dragged through the water.

Postflight examination of the airplane revealed a broken outboard left horizontal stabilizer tube which the pilot believed occurred during the wake encounter. It also revealed that the bolt connecting the three stabilizer cables had torn into the fabric, which the pilot surmised resulted in binding the control stick in a pitch-up position upon rotation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA13LA198