Summary
On June 09, 2013, a Beech C24R (N1854P) was involved in an incident near Peyton, CO. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot’s failure to maintain proper pitch control during takeoff.
During takeoff, when the airplane reached the rotation speed, the pilot applied back pressure to the flight controls. When the airplane reached an altitude about 50 feet above the ground, the stall warning horn sounded. The pilot attempted to maintain airspeed and then executed a forced landing to a field straight ahead. The airplane touched down in the field, continued through a small wire fence, struck an embankment, and came to rest near a highway. The airplane received substantial damage to the wings and fuselage. The pilot reported a total of 6.1 hours in the airplane make/model and 71.4 hours in all aircraft. The pilot reported that there were no mechanical malfunctions or failures of the engine or airframe that would have precluded normal operation.
This incident is documented in NTSB report CEN13CA334. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N1854P.
Accident Details
Probable Cause and Findings
The pilot’s failure to maintain proper pitch control during takeoff.
Aircraft Information
Registered Owner (Historical)
Analysis
During takeoff, when the airplane reached the rotation speed, the pilot applied back pressure to the flight controls. When the airplane reached an altitude about 50 feet above the ground, the stall warning horn sounded. The pilot attempted to maintain airspeed and then executed a forced landing to a field straight ahead. The airplane touched down in the field, continued through a small wire fence, struck an embankment, and came to rest near a highway. The airplane received substantial damage to the wings and fuselage. The pilot reported a total of 6.1 hours in the airplane make/model and 71.4 hours in all aircraft. The pilot reported that there were no mechanical malfunctions or failures of the engine or airframe that would have precluded normal operation.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN13CA334