Accident Details
Probable Cause and Findings
The pilot’s failure to establish and maintain a positive climb rate during the initial climb in night instrument meteorological conditions.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn August 3, 2013, at 0456 central daylight time, a Cirrus SR22, N225CD, was destroyed when it impacted trees and terrain about 0.6 nautical miles (nm) west of the Spirit of St. Louis Airport (SUS), Chesterfield, Missouri. The wreckage was fragmented and a post impact ground fire consumed a majority of the airplane. The airplane was departing from SUS and was en route to the Dalhart Municipal Airport (DHT), Dalhart, Texas. The private pilot and one passenger received fatal injuries. The airplane was registered to 225CD LLC and operated by the pilot under the provisions of the 14 Code of Federal Regulations as a Part 91 personal flight. Night instrument meteorological conditions (IMC) prevailed at the time of the accident, and an instrument flight plan was filed.
At 0321, the pilot contacted the Fort Worth Automated Flight Service Station (FSS) to receive a standard weather briefing. The FSS briefer provided information about the instrument flight rules (IFR) conditions that prevailed at SUS and would be in effect for much of the morning. IFR and low IFR conditions prevailed throughout central Missouri and Kansas. The pilot decided to file an IFR flight plan that would proceed from SUS to St. Joseph, Missouri, and then proceed to the southwest to land at DHT for fuel. Visual meteorological conditions prevailed between DHT and the pilot's final destination, the Winslow-Lindbergh Regional Airport (INW), Winslow, Arizona.
At 0451, the pilot contacted the St. Louis Terminal Radar Approach Control Facility (TRACON) to obtain a departure clearance, since the control tower at SUS was not open. The pilot was cleared to DHT as filed in his flight plan. He was cleared to climb to 3,000 feet above mean sea level (msl), and to expect 10,000 feet msl 10 minutes after departure. At 0452, the TRACON controller told the pilot he was released for departure, and when able, to proceed on course. He requested that the pilot call him if his departure was delayed more than five minutes. The pilot responded, "Will call you back if, ah, more than five minutes, Five Charlie Delta. Cleared for departure." There were no further communications from the pilot.
Approach control radar data indicated that the airplane became airborne about 0456. The first four radar returns indicated that the airplane climbed to 600 feet msl +/- 50 feet. The fifth radar return indicated the airplane was at 500 feet msl +/- 50 feet. The last radar return was about 0.3 nm from the departure end of runway 26R. The elevation at SUS is 463 feet.
A witness reported that he was driving south on N. Eatherton Road, which runs perpendicular to runway 26R about 0.3 nm west of the departure end of runway 26R, and observed seeing the accident airplane's navigation lights for about 3 to 5 seconds as it traveled to the west. The airplane appeared to be traveling at a high rate of speed and in about a 20 degree descent. He saw a fireball as the accident airplane impacted the trees and terrain. He reported that the weather conditions were "very foggy," and it was the worst fog conditions that he had observed for the year. He reported that he could only see the accident airplane's navigation lights due to the fog and light conditions. PERSONNEL INFORMATIONThe 41-year-old private pilot held a single-engine land and airplane instrument ratings. He received his airplane instrument rating on February 14, 2013, and he used the accident airplane for his instrument training and instrument check ride. He held a third class medical certificate. The pilot's logbook was not retrieved; however, aircraft flight logs and insurance records indicated that the pilot had about 475 total flight hours with about 154 hours in accident airplane. He flew about 24 hours within the last 30 days. The pilot's total number of instrument hours flown is unknown. He pilot purchased a 1/3 ownership in the accident airplane about 1.5 years before the accident.
The pilot's instrument instructor reported that he provided about 20 hours of training in preparation for the pilot's instrument rating. He stated the accident pilot was quick to engage the autopilot and was overly trusting of the autopilot system at the beginning of their training. He worked with the pilot to hand fly the airplane to increase his skill level in instrument conditions. He never flew with the accident pilot in actual IMC, but they flew several flights at night.
The designated pilot examiner who gave the instrument check ride to the pilot reported that the pilot failed his first check ride in January 2013. The pilot reportedly had deviated off course while on an instrument landing system (ILS) and GPS instrument approaches during the first check ride attempt. He stated that the accident pilot met all the standards of the practical test during the second check ride, and was issued his instrument rating in February 2013.
The pilot's wife reported that he had been on vacation since Wednesday, July 31, 2013. He had normal sleep cycles on account that he did not have to go to work. The pilot did not have any sleep deprivation problems, was healthy, and typically exercised every day. He loaded the airplane on Friday night in order to get an early departure on Saturday morning. The pilot's wife was uncertain how much sleep he had on Friday night. AIRCRAFT INFORMATIONThe airplane was a single-engine Cirrus SR22, serial number 0031. The engine was a Continental 310-horsepower IO-550N engine. The airplane seated four and had a maximum gross weight of 3,400 pounds. The last annual maintenance inspection was conducted on September 11, 2012, with a total time of 1800.8 hours on the airframe and engine. The last oil change was completed on July 21, 2013, with an engine time of 2,067.4 hours. An engine oil analysis indicated normal values at the last inspection.
On July 18, 2013, an Avidyne EX5000 Multifunction Display (MFD), part number 700-00004-006, serial number 2055, was installed on the airplane. The original ARNAV MFD was providing erroneous information and required replacement. The total airframe time was 2,058.1 hours.
On July 31, 2013, the pilot altimeter, static pressure system, transponder, and altitude encoder were tested and certified. The total airframe time at the time of the inspection was 2,074.8 hours.
One of the partners who owned the airplane reported that he flew the airplane to Joplin, Missouri, and back to SUS on the day before the accident. He encountered some IMC conditions during the flight and used the autopilot for the entire flight, except for the takeoffs and landings. He stated that all the instruments were working properly for the flight, and for the 4 to 5 flights he had flown during the last 10 days. He stated that he had flown the airplane a dozen times since the MFD was replaced and it operated properly during those flights. METEOROLOGICAL INFORMATIONThe SUS weather surface observation at 0454 was: wind 010 at 4 knots; visibility 3 miles in mist; overcast ceiling at 400 feet above ground level (agl), temperature 22 degrees Celsius (C); dew point 21 degrees C; altimeter 29.95.
The SUS special weather surface observation at 0512 was: wind 020 at 7 knots; visibility 1 3/4 miles in mist; overcast ceiling at 400 feet agl, temperature 22 degrees C; dew point 21 degrees C; altimeter 29.95; ceilings variable from 200 to 600 feet. AIRPORT INFORMATIONThe airplane was a single-engine Cirrus SR22, serial number 0031. The engine was a Continental 310-horsepower IO-550N engine. The airplane seated four and had a maximum gross weight of 3,400 pounds. The last annual maintenance inspection was conducted on September 11, 2012, with a total time of 1800.8 hours on the airframe and engine. The last oil change was completed on July 21, 2013, with an engine time of 2,067.4 hours. An engine oil analysis indicated normal values at the last inspection.
On July 18, 2013, an Avidyne EX5000 Multifunction Display (MFD), part number 700-00004-006, serial number 2055, was installed on the airplane. The original ARNAV MFD was providing erroneous information and required replacement. The total airframe time was 2,058.1 hours.
On July 31, 2013, the pilot altimeter, static pressure system, transponder, and altitude encoder were tested and certified. The total airframe time at the time of the inspection was 2,074.8 hours.
One of the partners who owned the airplane reported that he flew the airplane to Joplin, Missouri, and back to SUS on the day before the accident. He encountered some IMC conditions during the flight and used the autopilot for the entire flight, except for the takeoffs and landings. He stated that all the instruments were working properly for the flight, and for the 4 to 5 flights he had flown during the last 10 days. He stated that he had flown the airplane a dozen times since the MFD was replaced and it operated properly during those flights. WRECKAGE AND IMPACT INFORMATIONThe examination of the accident site revealed that the accident airplane impacted the woods located west of SUS on a 250 degree magnetic heading from the departure end of runway 26R. The wreckage path was about 350 feet in length, also on about a 250 degree magnetic heading, from where the initial impact occurred at the edge of the woods to the nose landing gear, which was the part of the accident airplane found furthest from the initial impact point.
A piece of the right wingtip was observed embedded in the trunk of a 70 to 80 foot tall tree located near the edge of the woods. The piece was embedded about 30 feet up from the base of the tree. Another tree about 96 feet from the initial impact point also was struck. The tree was about 32 inches in diameter at the base of the tree. The impact occurred near the tree's mid-span and the impact toppled the top of the tree in the direction of travel. A piece of the tree trunk was found at the base of the tree that had a 13 inch by 18 inch diagonal slash with gray paint transfer, which wa...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN13FA456