Accident Details
Probable Cause and Findings
The partial loss of engine power due to an improperly maintained carburetor and the pilot's subsequent failure to maintain aircraft control.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn April 11, 2014, at 1007 Pacific daylight time, an experimental amateur-built Bowers (Williams Myron G) Fly Baby 1A, N6054Q, collided with wooded terrain near Mariposa, California. The airplane was registered to, and operated by, the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. The commercial pilot sustained fatal injuries; the airplane sustained substantial damage to the forward fuselage and both wings during the accident sequence. The local flight departed Mariposa-Yosemite Airport, Mariposa, about 0950. Visual meteorological conditions prevailed, and no flight plan had been filed.
A witness located about 3 miles northwest of Mariposa Airport, was outside and observed an airplane approaching from the southeast flying at an altitude of about 1,000 feet above ground level (agl). The airplane began a left turn as it approached, and appeared to be descending. He described the engine as making a "missing" sound, as if power was intermittently being interrupted. The airplane then began a right turn, arcing around his location, and by the time it had passed behind him, it had descended to an altitude of about 300 feet agl. It then gradually rolled out of the turn and proceeded to fly towards the hills to the northeast. By then, the engine sound appeared muffled, and the airplane appeared to have slowed down considerably. The nose began to pitch up to about 30 degrees, almost parallel with the slope of the hill, as the airplane disappeared out of the witness's view behind trees. He did not hear any other sounds, but assumed the airplane had crashed. He then asked a family member to call 911; dispatch records from the Mariposa County Sheriff department revealed that the call was made at 1008. PERSONNEL INFORMATIONThe 80-year-old-pilot held a commercial pilot certificate with ratings for airplane single-engine land, and instrument airplane issued in 1972. His most recent Federal Aviation Administration (FAA) third-class medical certificate was issued in October 2007, with limitations that he possess glasses that correct for near vision. At the time of his last medical application, the pilot reported a total flight time of 1,800 hours.
An entry in the pilot's flight logbook dated June 22, 2013, indicated that he had received 0.6 hours of flight training with an instructor in a Cessna 152, practicing "maneuvers, stalls, slow flight"; however, the most recent documented flight review was completed in November 2007. According to the logbook, his total flight experience in the two year period preceding the accident was 15.1 hours. His total experience in the accident airplane was 3.1 hours, all of which occurred during 4 flights in the month leading up to the accident. AIRCRAFT INFORMATIONThe plans-built, single-seat, low-wing airplane's primary structure was comprised of wood covered in fabric, with the wings and landing gear braced by steel wires. The airplane was powered by a four-cylinder Continental A65-8 engine, and equipped with a wooden two-blade propeller.
The airplane was issued its special airworthiness certificate on October 20, 2006, and that same day, was involved in an accident after losing power on its maiden flight. The pilot/builder self-reported that the loss of power was most likely caused by his failure to use carburetor heat, and the NTSB determined the probable cause of the accident to be, "a loss of engine power due to the pilot's failure to use carburetor heat during conditions that were conducive to carburetor icing."
The airplane was sold to the accident pilot in December 2012, with maintenance logbooks indicating that it had accrued a total of 29 flight hours. The logbooks indicated that over the next 3 months the pilot performed a series of repairs to the brakes, control surfaces, and flying cables, as well as replacing the propeller and right magneto cap. The pilot reported to a friend that the build quality of the airplane was "crude," and that he intended to progressively restore the airplane to an airworthy condition.
The airplane subsequently underwent a series of taxi tests in March 2013, but was not flown for the remainder of the year. On March 3, 2014, an annual inspection was completed by an FAA certified airframe and powerplant mechanic, who held an inspection authorization rating. The mechanic stated that prior to his examination the engine was backfiring, and the pilot had not been able to successfully resolve the problem. The mechanic subsequently discovered that the magneto leads to two cylinders had been transposed.
The first flight followed shortly thereafter, and according to the pilot's friend, was an accidental flight when the airplane broke ground during a high speed taxi test. About 2 weeks prior to the accident, the pilot performed an intentional flight test. During that flight he experienced flight control difficulties in roll. He also stated that the airplane's airspeed indicator was not performing consistently, and that he planned to move the Pitot tube further outboard on the wing, away from the propeller slipstream. METEOROLOGICAL INFORMATIONThe closest weather reporting station at an elevation similar to the accident site was located at Columbia Airport, Columbia, California; this was situated about 36 miles north-northwest of the accident location. The 1015 Columbia automated report indicated calm wind, sky clear, temperature of 23 degrees C, dew point 06 degrees F, and an altimeter setting at 29.93 inches of mercury. AIRPORT INFORMATIONThe plans-built, single-seat, low-wing airplane's primary structure was comprised of wood covered in fabric, with the wings and landing gear braced by steel wires. The airplane was powered by a four-cylinder Continental A65-8 engine, and equipped with a wooden two-blade propeller.
The airplane was issued its special airworthiness certificate on October 20, 2006, and that same day, was involved in an accident after losing power on its maiden flight. The pilot/builder self-reported that the loss of power was most likely caused by his failure to use carburetor heat, and the NTSB determined the probable cause of the accident to be, "a loss of engine power due to the pilot's failure to use carburetor heat during conditions that were conducive to carburetor icing."
The airplane was sold to the accident pilot in December 2012, with maintenance logbooks indicating that it had accrued a total of 29 flight hours. The logbooks indicated that over the next 3 months the pilot performed a series of repairs to the brakes, control surfaces, and flying cables, as well as replacing the propeller and right magneto cap. The pilot reported to a friend that the build quality of the airplane was "crude," and that he intended to progressively restore the airplane to an airworthy condition.
The airplane subsequently underwent a series of taxi tests in March 2013, but was not flown for the remainder of the year. On March 3, 2014, an annual inspection was completed by an FAA certified airframe and powerplant mechanic, who held an inspection authorization rating. The mechanic stated that prior to his examination the engine was backfiring, and the pilot had not been able to successfully resolve the problem. The mechanic subsequently discovered that the magneto leads to two cylinders had been transposed.
The first flight followed shortly thereafter, and according to the pilot's friend, was an accidental flight when the airplane broke ground during a high speed taxi test. About 2 weeks prior to the accident, the pilot performed an intentional flight test. During that flight he experienced flight control difficulties in roll. He also stated that the airplane's airspeed indicator was not performing consistently, and that he planned to move the Pitot tube further outboard on the wing, away from the propeller slipstream. WRECKAGE AND IMPACT INFORMATIONThe airplane came to rest at the base of an oak tree, within densely wooded terrain at an elevation of 2,250 feet mean sea level (msl), about 3 miles northwest of Mariposa Airport. The terrain surrounding the accident site was comprised of grass and poison oak, interspersed with rocky outcroppings and various oak trees ranging in height from saplings to 20 feet tall. The airplane came to rest on a magnetic heading of about 60 degrees, facing uphill on a 20-degree slope. A freshly cut swath through the tree branches was located directly above the airplane; the swath was nearly vertical. Although the airplane was surrounded by trees, no other damage to limbs or branches was noted.
The wings came to rest inverted, with the forward fuselage and engine located underneath the wing root. The tailcone and empennage structure had separated aft of the seat, and was resting undamaged on its right side. Both wings sustained aft crush damage to their leading edges. The entire cabin structure forward of the tailcone was fragmented, and the firewall was compressed against the rear of the engine. All cockpit flight controls exhibited varying degrees of bending damage, but remained functionally intact. The fuel tank sustained multiple breaches, and was detached but still located within the center section of the wreckage.
The airframe and engine did not display any indications of bird strike or fire.
The engine remained attached to its mount, which remained attached to the firewall. Both magnetos (Eisemann, Model AM-4) remained firmly attached to the engine, however, their plug caps had both fragmented, crushing and exposing the timing gears, points, and coils, as well as detaching all ignition wires and both P-leads.
The carburetor had broken away from the inlet manifold, and the inlet air filter assembly exhibited crush damage. The throttle cable was attached and continuous from the cockpit to the butterfly valve; the cable was in the full-forward position at the cockpit control. The carburetor heat control cable was continuous from the cockpit control to th...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR14FA165