N166DR

Substantial
None

BELL/GARLICK UH 1HS/N: 66-16949

Accident Details

Date
Thursday, February 19, 2015
NTSB Number
WPR15LA109
Location
Shelton, WA
Event ID
20150220X74821
Coordinates
47.129444, -123.231109
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The fatigue failure of the engine-to-transmission driveshaft adapter attachment bolt due to the application of inadequate torque on the bolt during assembly.

Aircraft Information

Registration
Make
BELL/GARLICK
Serial Number
66-16949
Engine Type
Turbo-shaft
Year Built
1995
Model / ICAO
UH 1HUH1
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
15
FAA Model
UH-1H

Registered Owner (Current)

Name
OAS2 LLC
Address
235 NILSON WAY
City
ORLANDO
State / Zip Code
FL 32803-6488
Country
United States

Analysis

On February 19, 2015, about 1300 Pacific standard time, a Bell/Garlick UH 1H Helicopter, N166DR, made an emergency landing and rolled over following a loss of engine power while in a hover near Shelton, Washington. Northwest Helicopters, Inc., was operating the helicopter under the provisions of 14 Code of Federal Regulations Part 137. The commercial pilot received minor injuries, the helicopter was substantially damaged. Visual meteorological conditions prevailed, and no flight plan had been filed.

The pilot reported that while in a hover and beginning to lift a 3,000-pound agricultural application container, he heard a "loud bang" followed by the low rotor warning horn sounding. The pilot pulled away from ground crew as the helicopter yawed to the left. He was able to keep the helicopter level about 5 to 7 ft above the ground when he pulled the remaining collective pitch to touch down. The ground underneath was uneven and the helicopter subsequently rolled over onto its right side.

During the postaccident wreckage examination, the engine to transmission driveshaft adapter (Part Number 204-040-812-3), was found broken in multiple pieces. The driveshaft adapter is the component between the engine output and the driveshaft. The failed components were recovered and sent to the National Transportation Safety Board Materials Laboratory Division for further examination.

The Materials Engineer reported that thumbnail-shaped patterns and progressive crack arrest marks consistent with fatigue were observed on the fracture surfaces. The bolt that attached the driveshaft adapter to the mating coupling set had separated. The fracture surfaces on the bolt were generally flat, with progressive crack arrest lines consistent with fatigue cracking.

Bell Helicopter Alert Service Bulletin No. 204-77-6 dated September 30, 1977, Inspection of Engine Drive Shaft Adapter Bolt, P/N 204-040-813-001 for loss of torque, and Technical Bulletin No. 204-81-18 dated June 10, 1981, Engine Driveshaft Adapter P/N 204-040-812-003 rework, indicated that considerable fretting wear damage had occurred to the engine output adapter plug, P/N 1-030-360-04 when engines were returned for overhaul. Extensive wear will allow the drive shaft adapter, P/N 204-040-812-003, to seat on the anti-rotation tangs of the plug and result in a false torque of bolt, P/N 204-040-813-001. The condition will cause plug wear and reduction gear damage. The fretting wear damage of the plug will be eliminated by maintaining the required torque of 160-200 inch-pounds on bolt, P/N 204-040-813-001. Both bulletins recommend compliance times to minimize fretting wear and damage. (See public docket for more information).

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR15LA109