N7770Q

Substantial
None

CESSNA 310QS/N: 310Q0270

Accident Details

Date
Saturday, March 21, 2015
NTSB Number
WPR15LA129
Location
St. George, UT
Event ID
20150323X03212
Coordinates
37.091667, -113.592781
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

Failure of the left main landing gear lower adjusting bolt due to overstress, which resulted in the left main landing gear collapse during landing.

Aircraft Information

Registration
N7770Q
Make
CESSNA
Serial Number
310Q0270
Engine Type
Reciprocating
Year Built
1971
Model / ICAO
310QC310
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
SALE REPORTED
Address
3011 W BUCKEYE RD
Status
Deregistered
City
PHOENIX
State / Zip Code
AZ 85009-5734
Country
United States

Analysis

On March 20, 2015, about 1900 mountain daylight time, a Cessna 310Q airplane, N7770Q, experienced a left main gear collapse during the landing roll at St. George Regional Airport (SGU), St. George, Utah. The commercial pilot and one passenger were not injured; the airplane sustained substantial damage to the left aileron. The airplane was registered to, and operated by, the pilot as a 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed, and no flight plan was filed. The flight departed SGU about 1800.

The pilot reported that the purpose of this flight was to regain currency after the airplane had been in maintenance for an extended period of time. During the flight, three takeoff and landings were completed before the pilot departed the traffic pattern to practice inflight maneuvers. After finishing the maneuvers, he reentered the traffic pattern for landing. With normal landing gear indications in the cockpit, the pilot landed the airplane normally and uneventfully. During the landing roll, the left wing lowered more than normal; subsequently, the engine propellers and wingtip impacted the runway surface. The airplane slowly slid to the left and exited the runway surface.

A postaccident examination conducted by a Federal Aviation Administration Inspector revealed that the lower adjusting bolt on the left main landing gear was fracture separated. High quality photos of the fracture surfaces were sent to the National Transportation Safety Board (NTSB) Materials Laboratory for further examination. The NTSB Materials Laboratory specialist reported that both fracture surfaces exhibited fractographic features consistent with overstress fracture due to tensile and cantilever bending loads applied to the tie-rod end fitting. No indications of preexisting cracking was observed.

Review of maintenance logbooks revealed the last annual inspection was completed the same day as the accident. During the inspection, the left and right landing gear side brace bolts and bushings were replaced, and a gear retraction test was satisfactory.

According to a Cessna Representative, the area of the fracture is where a mechanic would place the spring scale to measure the down lock force. This area is one of two main fracture locations when the down lock is improperly adjusted.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR15LA129