N8401N

Substantial
None

BEECH E33AS/N: CE-215

Accident Details

Date
Thursday, June 11, 2015
NTSB Number
WPR15LA183
Location
Tucson, AZ
Event ID
20150614X35207
Coordinates
32.446666, -111.002777
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A loss of left braking action for reasons that could not be determined because postaccident examination did not reveal any evidence of preimpact mechanical failures or malfunctions that would have precluded normal operation, which resulted in a loss of directional control.

Aircraft Information

Registration
Make
BEECH
Serial Number
CE-215
Engine Type
Reciprocating
Year Built
1968
Model / ICAO
E33ABE33
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
E33A

Registered Owner (Current)

Name
N8401N LLC
Address
72275 ROAD 410
City
CAMBRIDGE
State / Zip Code
NE 69022-3606
Country
United States

Analysis

On June 11, 2015, about 0840 mountain standard time, a Beech E33A, N8401N, exited the runway landing surface during the landing rollout at La Cholla Airpark, Tucson, Arizona, and collided with a drainage ditch. The owner/pilot was operating the airplane under the provisions of 14 Code of Federal Regulations Part 91. The commercial pilot was not injured; the airplane sustained substantial damage. The local personal flight departed Tucson, about 0800. Visual meteorological conditions prevailed, and no flight plan had been filed.

In a written statement, the pilot reported that the landing touchdown was smooth, with power nearly off. During the landing roll, he applied gentle pressure to the brakes to slow down, however the left side braking action was non-existent, while the right side brake held. The pilot was unable to maintain directional control as the airplane departed the narrow runway and subsequently collided with a drainage ditch and low cement wall.

The wreckage was recovered to a secured facility where a Federal Aviation Administration Inspector from the Scottsdale, Arizona, Flight Standards District Office examined the brake system. The inspector reported no evidence of a mechanical malfunction or failure. The hydraulic system was almost empty due to the bleeder valve on the brake caliper was sheared off.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR15LA183